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时间:2011-04-01 19:20来源:蓝天飞行翻译 作者:航空
曝光台 注意防骗 网曝天猫店富美金盛家居专营店坑蒙拐骗欺诈消费者

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 27-51-00
 ALL  ú ú 01 Page 107 ú Nov 15/96
BOEING PROPRIETARY - Copyright (C) - Unpublished Work - See title page for details.
A 737-300/400/500MAINTENANCE MANUAL
TROUBLE  PROBABLE CAUSE  ISOLATION PROCEDURE  REMEDY 
operation Slow or fast flap tion Slow flap opera-not electrically hydraulically but Flaps operate  ority valve Defective pri-tion (Position 1) assembly or transmission Binding gearbox No ac power switches alternate flap No dc power at limit switch Defective flap in normal posi-Flap bypass valve unit alternate drive Defective flap  (Ref 27-51-84, R/I) Shooting normal operating time Check trailing edge flaps flap transmission and check for free rotation each side of gearbox or Disconnect torque tubes on Electrical Power - Trouble Refer to Chapter 24, for continuity through circuit breakers nate flaps switches Check circuit from alter-through flap limit switch Check circuit continuity sent, valve is defective valve. If power is pre-for power at flap bypass With switch at ARM, check master switch is at ARM. and that alternate flap circuit breaker is closed Check that FLAP VALVES unit is defective power is present, drive alternate drive unit. If Check for power at flap  (Ref 27-51-87, 27-51-84, R/I) 27-51-82, R/I) 27-51-59, R/I) valve (Ref Replace priority Shooting Chart) this Trouble electrically (in hydraulically or not operate See flaps will breaker switch or circuit replace defective Repair wiring or R/I) limit switch Replace flap valve (Ref Replace bypass unit (Ref alternate drive Replace flap 

EFFECTIVITYùùùùùùùùùùùùùùùùùùùùùùùùùùùùùù. ú

 27-51-00
 ALL  ú ú 01 Page 108 ú Nov 15/96
BOEING PROPRIETARY - Copyright (C) - Unpublished Work - See title page for details.
A 737-300/400/500MAINTENANCE MANUAL
TROUBLE  PROBABLE CAUSE  ISOLATION PROCEDURE  REMEDY 
Loose control  Low cable tension  Check cable tension per  Adjust cable 
cables  Broken control cable  AMM 27-51-00/501 Check cable run for broken cable  tension Replace broken cable 
Flap position  Flap position  Check that trailing edge  Rerig flap posi-
indicator  indicator system  flap position indicating  tion indicating 
pointers stop  out of rig  system is in adjustment  system 
between 15 and 25  (AMM 27-58-01/ 
units, when 25  501) 
units of flaps is selected, but continue toward 40 units when 40 units is selected  cator position indi-Faulty flap  Both flap position indi-cator pointers do not indicate selected units  401) (AMM 27-58-41/ Replace flap posi-tion indicator 
Faulty flap position trans-mitter  One flap position indi-cator pointer does not indicate selected units of flap position  401) (AMM 27-58-12/ mitter Replace flap position trans-
Flap position  Faulty flap  Perform flap asymmetry  Replace flap 
indicator  position indi- shutoff test  position indi-
pointers left and  cator  (AMM 27-51-00/501)  cator 
right are split and at the same time the primary flap drive system continues to  relay, R123 Faulty flap asymmetry shutoff  relay, R123 asymmetry shutoff Replace flap 401) (AMM 27-58-41/ 
operate. 

EFFECTIVITYùùùùùùùùùùùùùùùùùùùùùùùùùùùùùù. ú

 27-51-00
 ALL  ú ú 02 Page 109 ú Jul 15/96
BOEING PROPRIETARY - Copyright (C) - Unpublished Work - See title page for details.
A 737-300/400/500MAINTENANCE MANUAL
TROUBLE  PROBABLE CAUSE  ISOLATION PROCEDURE  REMEDY 
Flaps do not  Flap load relief  Reset circuit 
retract auto- circuit breaker  breaker on panel 
matically from  open  P6 
light (not on FLAP LOAD RELIEF 162 knots and exceeds 152 to when airspeed 40- to 30-units  supply PC board) receiver or power ARINC 429 Faulty airspeed switches (or  on Check that test light comes LOAD LIMITER TEST light. Verify squat switch is operating. Press-to-test  Replace squat switch 
 
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本文链接地址:737-300 400 500 AMM 飞机维护手册 飞行操纵 FLIGHT CONTROLS 3(147)