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时间:2011-04-02 15:00来源:蓝天飞行翻译 作者:航空
曝光台 注意防骗 网曝天猫店富美金盛家居专营店坑蒙拐骗欺诈消费者

 |  transfer between|  |  trouble shooting  |  procedure for |
 |  systems A and B|  |  fluid transfer  |  operating |
 |  or B and A|  |  |  hydraulic |
 |  |  |  |  powered systems|
 |  |  |  |  or replace |
 |  |  |  |  parts |
 |  |  |  |  |

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 29-15-00
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 ú  02  Page 104
 ú  Nov 12/01 

BOEING PROPRIETARY - Copyright (C) - Unpublished Work - See title page for details.
A
737-300/400/500MAINTENANCE MANUAL
 ~............................................................................... | TROUBLE | PROBABLE CAUSE | ISOLATION PROCEDURE | REMEDY | ................................................................................. | |Fluid shrinkage | (AMM 12-12-00/301)| | | |during cold| | | | |conditions| | | | | | | | | Hydraulic |Hydraulic fluid | See the steps for | Use the correct| | fluid comes |transfer between | trouble shooting | procedure for| | out of the |systems A and B | fluid transfer. | operating| | reservoir |or B and A | | the hydraulic| | vent line | | | powered systems| | | | | or replace the| | | | | bad parts.| | | | | | | |Fluid quantity | Do the Inspection | Replace the| | |indicator on the | procedure for the fluid | fluid quantity| | |reservior | quantity indicator | indicator| | | | (AMM 29-33-12/601). | (AMM| | | | | 29-33-12/401).| | | | | | | Hydraulic |High pressure | Depressurize and | Replace| | fluid |leakage through | disconnect system A | brake| | transfer from brake shuttle| | pressure line from | shuttle| | system B to A valve/s| | each of the four | valve| | | | brake shuttle valve| | | | | lines. Pressurize| | | | | system B. Leakage| | | | | from any brake| | | | | shuttle valve is| | | | | causing the problem.| | | | | | | | | | | | | |Low pressure | Can occur on airplanes | Consider| | |(return system) | prior to incorporation | incorporating| | |leakage through | of SB 737-29-1065, due | the balance| | |brake shuttle | to differences between | line| | |valve (On | reservoir pressures. | modification| | |airplanes not | | (SB| | |incorporating | | 737-29-1065)| | |the balance line| | | | |modification,| | | | |SB 737-29-1065)| | | | | | | | | | | | | | |Incorrect | Fluid transfer caused by | AMM| | |parking brake | setting brakes using | 12-12-00/301| | |pre-start | system B and releasing| | | |procedure | brakes using system A while| | | | | system B is depressurized| | | | | | |
 EFFECTIVITYùùùùùùùùùùùùùùùùùùùùùùùùùùùùùù. ú
 29-15-00
 ALL ú

 ú 01 Page 105 ú Nov 12/01
BOEING PROPRIETARY - Copyright (C) - Unpublished Work - See title page for details.
A
737-300/400/500MAINTENANCE MANUAL
 ~............................................................................... | TROUBLE | PROBABLE CAUSE | ISOLATION PROCEDURE | REMEDY | .................................................................................
 |  Incorrect|  |  Fluid transfer is caused  |  Use correct|
 |  thrust|  |  when left thrust reverser  |  procedures|
 |  reverser|  |  is actuated by standby  |  for operating|
 |  actuation|  |  hydraulic system  |  thrust|
 |  |  |  |  reverser|
 |  |  |  |  (AMM 29-15-00).|
 |  |  |  |  Make sure no|
 |  |  |  |  fluid transfers|
 |  |  |  |  when operating|
 |  |  |  |  thrust|
 |  |  |  |  reverser by|
 |  |  |  |  normal|
 |  |  |  |  procedure|
 |  |  |  |  |
 |  Defective|  |  If indicator is white,  |  Correct wiring|
 |  components|  |  verify continuity of wires  |  hook-up as|
 |  supplying|  |  between M1190 card (pins  |  necessary|
 |  power to|  |  27 and 28) and engine No. 1|  |
 |  landing gear|  |  N2 connector D552 (pins 4 |  |
 
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