EFFECTIVITYùùùùùùùùùùùùùùùùùùùùùùùùùùùùùù. ú
71-00-42
ALL ú
ú C01 Page 107
ú Nov 15/92
BOEING PROPRIETARY - Copyright (C) - Unpublished Work - See title page for details.
////////////////////////A / /
CFM56 ENGINES
737-300/400/500/ /MAINTENANCE MANUAL ////////////////////////
FROM SHEET 1 (BLOCK 5)
NO
NO
7 DO THE T2/CIT SENSOR TEST
37 REPLACE THE T2 SENSOR (AMM 71-00-00/501, TEST (AMM 73-21-09/401) OR THE CIT NO. 11).SENSOR (AMM 73-21-02/401) AS
ARE THE SENSORS SERVICE-APPLICABLE.
ABLE?
YES YES9
VISUALLY EXAMINE VSV
39 REPAIR/REPLACE THE
ACTUATION SYSTEM FOR DAMAGECOMPONENTS OR REPLACE THE
(AMM 72-35-00/601). ENGINE (AMM 71-00-02/401).
IS DAMAGE MORE THAN THE
LIMITS FOUND?
NO
NO
41 ADJUST THE VSV ACTUATORS (AMM 75-31-00/501), THEN ADJUST THE VSV FEEDBACK CABLE (AMM 75-31-02/501).
YES
NO
13 DO THE VSV FEEDBACK CABLE
STATIC RIGGING CHECK
(AMM 75-31-02/501).
IS THE RIGGING CHECK OK?
YES
NO
15 DO THE VBV FEEDBACK CABLE
STATIC RIGGING CHECK
(AMM 75-32-05/501).
IS THE RIGGING CHECK OK?
YES
YES
NO
SEE SHEET 3 (BLOCK 19)
Cannot Get Takeoff Power with PMC OFF; PMC ON OK or Cannot Get
Takeoff Power with PMC ON and PMC OFF
Figure 103 (Sheet 2)
B05157
EFFECTIVITYùùùùùùùùùùùùùùùùùùùùùùùùùùùùùù. ú
71-00-42
ALL ú
ú C01 Page 108
ú Nov 15/95
BOEING PROPRIETARY - Copyright (C) - Unpublished Work - See title page for details.
////////////////////////A / /
CFM56 ENGINES
737-300/400/500/ /MAINTENANCE MANUAL ////////////////////////
FROM SHEET 2
(BLOCK 17)
YES
NO
19 EXAMINE THE BLEED VALVE
49 REPLACE THE FUEL GEAR FUEL GEAR MOTOR (AMM 75-32-01/ MOTOR (AMM 75-32-02/401).
601).
IS THE FUEL GEAR MOTOR SERVICEABLE?
YES NO
20 DO THE THRUST LEVER TRAVEL
50 REPAIR/REPLACE THE THRUST
CHECK (AMM 71-00-59/101, LEVER CABLE (AMM 76-11-04/201)
FIG. 113).OR THRUST LEVER PUSH-PULL
IS THE TRAVEL CHECK OK? CABLE (AMM 76-11-07/401).
YES YES
21 DO THE AUTOTHROTTLE
SYSTEM OPERATIONAL TEST
(AMM 22-31-00/501).
IS THE A/T SYSTEM OPERA-TION CORRECT?
NO NO
23 DO THE PART POWER TRIM
CHECK (AMM 71-00-00/501, TEST
NO. 6).
ARE THE SPEEDS CORRECT?
YES
Cannot Get Takeoff Power with PMC OFF; PMC ON OK or Cannot Get
Takeoff Power with PMC ON and PMC OFF
Figure 103 (Sheet 3)
B05151
EFFECTIVITYùùùùùùùùùùùùùùùùùùùùùùùùùùùùùù. ú
71-00-42
ALL ú
ú C01 Page 109
ú Nov 15/93
BOEING PROPRIETARY - Copyright (C) - Unpublished Work - See title page for details.
////////////////////////A / /
CFM56 ENGINES
737-300/400/500/ /MAINTENANCE MANUAL ////////////////////////
PREREQUISITES NONE
NO
YES
NO
NO
29 REPLACE THE MEC (AMM 73-21-01/401).
27 ADJUST THE PMC PLA GAIN (AMM 73-21-00/501) AND/OR REPLACE THE FUEL CONTROL BOX (AMM 76-11-08/401).
CANNOT GET TAKEOFF POWER WITH PMC ON; PMC OFF OK
1
DO A CHECK OF THE PMC PART NUMBER.
IS THE PART NUMBER CORRECT FOR THE ENGINE MODEL?
YES
3 DO THE PS12 TUBE/MANIFOLD CHECK (AMM 71-00-59/101, FIG. 104).
ARE LEAKS/BLOCKAGE/DAMAGE FOUND?
NO
5 DO THE PMC AND RELATED
COMPONENTS TEST (AMM 73-21-00/
501).
IS THE PMC OPERATION CORRECT?
YES
7 DO THE PMC PLA RVDT
VOLTAGE CHECK (AMM 73-21-00/
501).
IS THE VOLTAGE CHECK CORRECT?
YES
Cannot Get Takeoff Power With PMC ON; PMC OFF OK
Figure 103A
EFFECTIVITYùùùùùùùùùùùùùùùùùùùùùùùùùùùùùù. ú 中国航空网 www.aero.cn 航空翻译 www.aviation.cn 本文链接地址:737-300 400 500 AMM 飞机维护手册 动力装置 POWER PLANT 2(9)