EFFECTIVITYùùùùùùùùùùùùùùùùùùùùùùùùùùùùùù. ú
 71-00-42
 ALL  ú 
 ú  C01  Page 145 
 ú  Jul 12/01 
BOEING PROPRIETARY - Copyright (C) - Unpublished Work - See title page for details. 
H03380
////////////////////////A / /
CFM56 ENGINES
737-300/400/500/ /MAINTENANCE MANUAL //////////////////////// 
THROTTLE STAGGER OR N1 IS NOT AT TARGET AT CLIMB OR CRUISE
NO 
NO
1 LOOK AT THE ENGINE INLET 
21 IF FOD IS FOUND, DO THE
AND EXHAUST AREAS FOR OBVIOUS BIRDSTRIKE/FOD TROUBLESHOOTING 
SIGNS OF DAMAGE. (AMM 71-00-47/101).
DID YOU FIND FOREIGN IS THE FOD IN LIMITS? OBJECT DAMAGE (FOD) OR METAL 
YES
PARTICLES? IS THE ENGINE FOD FREE?
YES NO
2 MAKE SURE THE ENGINE TYPE/
43 MAKE SURE THE PIN THRUST RATINGS ARE CORRECT. SELECTION OF A/T AND FMC AGREE 
DO THIS PROCEDURE: A/T WITH THE CURRENT ENGINE(S) AND 
BITE - ENGINES/RATINGS THRUST RATING (PER WDM OR 
(AMM 22-04-10/101, FIG. 117). SB). 
ARE THE TESTS IN THE 
LIMITS?
YESNO3 LOOK AT THE T12 SENSOR IN
THE ENGINE INLET FOR DAMAGE/ 
DEFECTS (AMM 73-21-05/601).
 DID YOU CORRECT THE DEFECTS?
YES YES
4 DO THE PS12 TUBE/MANIFOLD
CHECK (AMM 71-00-59/101, 
FIG. 106).
 DID YOU FIND LEAKS OR DAMAGE?
NO NO
5 DISCONNECT PLUG D3010 FROM
46 REPLACE THE P5-68 PMC 
THE PMC AT J4 (WDM 73-24-11).PANEL (AMM 73-21-12/401).
MAKE SURE THE PMC SWITCH IS AT THE ON POSITION AND DO A CONTINUITY CHECK FROM SOCKET 7 TO SOCKET 8.
 IS THERE AN OPENING FROM SOCKET 7 TO SOCKET 8? 
YES 
SEE SHEET 3 (BLOCK 6) 
Throttle Stagger or N1 is Not at Target at Climb or Cruise 
Figure 117B (Sheet 2)
EFFECTIVITYùùùùùùùùùùùùùùùùùùùùùùùùùùùùùù. ú
 71-00-42
 ALL  ú 
 ú  C01  Page 146 
 ú  Jul 12/01 
BOEING PROPRIETARY - Copyright (C) - Unpublished Work - See title page for details. 
H03382
////////////////////////A / /
CFM56 ENGINES
737-300/400/500/ /MAINTENANCE MANUAL //////////////////////// 
FROM SHEET 2 (BLOCK 5)
YES 
NO
6 DO THE PMC PLA GAIN CHECK 
(AMM 73-21-00/501).
IS THE VOLTAGE CORRECT? 
YES NO
7 DO THE PMC AND RELATED COMPONENTS TEST 
(AMM 73-21-00/501) (TEST N1
SPEED SENSOR, N2 ALTERNATOR, 
T12, MEC'S RVDT). 
ARE THE COMPONENTS 
SERVICEABLE?
YES NO8 EXAMINE THE THRUST LEVER 
TO CONTROL BOX ADJUSTMENT FOR 
THE TWO ENGINES (AMM 76-11-00/ 
501). 
IS THE THRUST LEVER
TRAVEL/ALIGNMENT OK?
YES NO9 DO THE T2/CIT SENSOR 
TEST 11 (AMM 71-00-00/501). 
ARE THE SENSORS 
SERVICEABLE?
YES NO10 DO THE PART POWER TRIM
CHECK (AMM 71-00-00/501, 
TEST 6) TO CHECK THE %N2 AND 
%N1 RPM.
 IS %N2 RPM (PMC OFF) CORRECT?
YES 
SEE SHEET 4 (BLOCK 11)
22 ADJUST THE PMC PLA GAIN. 
IF NOT ADJUSTABLE, REPLACE THE PMC.
 ADJUSTABLE AFTER PMC REPLACEMENT?
NO
YES
48 REPLACE THE PMC (AMM 73-21-04/401) OR SELECT THE DEFECTED COMPONENT TO REPLACE PER AMM 73-21-00, FIG. 505.
SMALL VOLTAGE ERRORS DO NOT CAUSE MUCH THROTTLE STAGGER. THE VOLTAGE ERROR WOULD HAVE TO BE ALMOST ONE VOLT TO PRODUCE ONE KNOB OF THROTTLE STAGGER. A SMALL VOLTAGE ERROR IS PROBABLY NOT THE ONLY THING TO CAUSE A LARGE THROTTLE STAGGER. THE TROUBLESHOOTING SHOULD CONTINUE IF A SMALL VOLTAGE ERROR IS FOUND. 
49 ADJUST THE THRUST CONTROL FUEL PUSH-PULL CABLE (AMM 76-11-00/501).
50 REPLACE THE T2 SENSOR (AMM 73-21-09/401) OR REPLACE THE CIT SENSOR (AMM 73-21-02/ 401). 
Throttle Stagger or N1 is Not at Target at Climb or Cruise 
Figure 117B (Sheet 3)
EFFECTIVITYùùùùùùùùùùùùùùùùùùùùùùùùùùùùùù. ú
 71-00-42
 ALL  ú 
 ú  C01  Page 147 
 ú  Jul 12/01 
BOEING PROPRIETARY - Copyright (C) - Unpublished Work - See title page for details. 
H03387
////////////////////////A / /
 
中国航空网 www.aero.cn
航空翻译 www.aviation.cn
本文链接地址:737-300 400 500 AMM 飞机维护手册 动力装置 POWER PLANT 2(20)