9 DO THE VSV FEEDBACK CABLE
39 ADJUST THE VSV FEEDBACK STATIC RIGGING CHECKCABLE (AMM 75-31-02/501).
(AMM 75-31-02/501).
IS THE RIGGING CHECK CORRECT?
YES NO
10 DO THE VBV FEEDBACK CABLE
40 ADJUST THE VBV FEEDBACK STATIC RIGGING CHECKCABLE (AMM 75-32-05/501).
(AMM 75-32-05/501).
IS THE RIGGING CHECK CORRECT?
DO THE VSV ACTUATOR RIG CHECK (AMM 75-31-00/501), THEN(AMM 75-31-00/501). ADJUST THE VSV FEEDBACK CABLE IS THE RIG CHECK CORRECT? (AMM 75-31-02/501).
YES
YES
13 USE A BORESCOPE AND
EXAMINE THE BOOSTER, HPC 3RD-,
5TH- AND 9TH-STAGE BLADES,
COMBUSTION CHAMBER AND HPT BLADES (AMM 72-00-00/601). IS DAMAGE MORE THAN THE LIMITS FOUND?
NO
SEE SHEET 3 (BLOCK 14)
Slow/Hung Acceleration
Figure 101 (Sheet 2)
EFFECTIVITYùùùùùùùùùùùùùùùùùùùùùùùùùùùùùù. ú
71-00-42
ALL ú
ú C01 Page 104
ú Jul 15/98
BOEING PROPRIETARY - Copyright (C) - Unpublished Work - See title page for details.
////////////////////////A / /
CFM56 ENGINES
737-300/400/500/ /MAINTENANCE MANUAL ////////////////////////
FROM SHEET 2 (BLOCK 13)
NO
YES
14 CHECK LOW AND HIGH IDLE
TOLERANCES (AMM 71-00-00/501,
TEST 4).
IS ADJUSTMENT REQUIRED?
NO
NO
15 ONLY ON ENGINES WITH THE
5TH-STAGE START BLEED VALVE,
ADJUST THE MEC SPECIFIC
GRAVITY TO THE LOW END OF THE PERMITTED RANGE FOR THE FUEL (AMM 71-00-58/501, FIG. 103).
DOES THE PROBLEM CONTINUE?
YES
NO
16 ADJUST LOW AND HIGH IDLE
SPEED TO THE HIGH END OF
TOLERANCE (AMM 71-00-00/501,
TEST 4). DOES THE PROBLEM CONTINUE?
YES
NO
17 DO THE VSV DYNAMIC RIG
PROCEDURE (AMM 75-31-00/501).
ADJUST THE VSVs TO THE
OPEN LIMIT.
DOES THE PROBLEM CONTINUE?
YES
NO
CONTINUE TROUBLESHOOTING IF ADJUSTMENT WAS FOUND TO BE HIGH.
Slow/Hung Acceleration
Figure 101 (Sheet 3)
EFFECTIVITYùùùùùùùùùùùùùùùùùùùùùùùùùùùùùù. ú
71-00-42
ALL ú
ú C01 Page 105
ú Nov 15/98
BOEING PROPRIETARY - Copyright (C) - Unpublished Work - See title page for details.
////////////////////////A / /
CFM56 ENGINES
737-300/400/500/ /MAINTENANCE MANUAL ////////////////////////
MENT THRUST LEVER MOVE-NO RESPONSE TO PREREQUISITES ENGINE OPERATION CAN BE NECESSARY
CHECK (AMM 71-00-59/101, FIG. 113). IS THE TRAVEL CHECK COR-RECT? 1 DO THE THRUST LEVER TRAVEL NO CABLE (AMM 76-11-07/401). LEVER CABLE (AMM 76-11-04/201) OR THE THRUST LEVER PUSH-PULL 21 REPAIR/REPLACE THE THRUST
TEST (AMM 71-00-00/501, TEST (AMM 73-21-02/401) OR T2
NO. 11).SENSOR (AMM 73-21-09/401), AS ARE THE SENSORS SERVICE-APPLICABLE.
ABLE?
YES
No Response to Thrust Lever Movement
Figure 102
EFFECTIVITYùùùùùùùùùùùùùùùùùùùùùùùùùùùùùù. ú
71-00-42
ALL ú
ú C01 Page 106
ú Nov 15/92
BOEING PROPRIETARY - Copyright (C) - Unpublished Work - See title page for details.
////////////////////////A / /
CFM56 ENGINES
737-300/400/500/ /MAINTENANCE MANUAL ////////////////////////
PREREQUISITES ENGINE OPERATION CAN BE NECESSARY
CANNOT GET TAKEOFF POWER WITH PMC "OFF"; PMC "ON OK" OR CANNOT GET TAKEOFF POWER WITH PMC "ON" AND PMC "OFF"
IS BLOCKAGE OR DAMAGE FOUND?
NO
YES
3 DO THE PS12 TUBE/MANIFOLD
CHECK (AMM 71-00-59/101,
FIG. 106).
ARE LEAKS FOUND?
NO
YES
5 EXAMINE THE CDP AND CBP
TUBING, AND TUBE DRAIN HOLES,
FOR LEAKS, DAMAGE, OR BLOCKAGE
(AMM 71-00-59/101, FIG. 104 AND 105).
ARE LEAKS, DAMAGE, OR BLOCKAGE FOUND?
NO SEE SHEET 2 (BLOCK 7)
Cannot Get Takeoff Power with PMC OFF; PMC ON OK or Cannot Get
Takeoff Power with PMC ON and PMC OFF
中国航空网 www.aero.cn
航空翻译 www.aviation.cn
本文链接地址:737-300 400 500 AMM 飞机维护手册 动力装置 POWER PLANT 2(8)