(4000HA) AMM 36-11-52-000-040 Removal of the Bleed Pressure-Regulator Valve (4001HA) AMM 36-11-52-400-040 Installation of the Bleed Pressure-Regulator Valve
(4001HA) ASM 36-11/02 TSM 36 PB 101
3. Fault Confirmation
__________________
A. Test
(1) Do the BITE test of the BMC2 (Ref. AMM TASK 36-11-00-740-001).
4. Fault Isolation
_______________
A. If the test gives a maintenance message, you can find the related trouble shooting procedure in the (Ref. TSM 36 PB 101).
(1) If there is no maintenance message:
-replace the VALVE-HP BLEED (4000HA) (Ref. AMM TASK 36-11-51-000-040) and (Ref. AMM TASK 36-11-51-400-040).
(a) If the fault continues:
-do the functional test of the upstream sense line between the bleed pressure-regulator valve (4001HA) and the control solenoid (10HA2) (Ref. AMM TASK 36-11-00-720-007).
1
-EFF : ALL
-∞∞36-11-00∞∞∞∞∞∞∞∞∞∞Page A288
--Feb 01/05R ---CES -
1 If the pressure decreases to 0 psig in less than 20 seconds:
_ -replace the related sense line.
2 If the pressure drop is not high:
_
-replace the VALVE-BLEED PRESS REG (4001HA) (Ref. AMM TASK 36-11-52-000-040) and (Ref. AMM TASK 36-11-52-400-040).
a If the fault continues:
_
-do a check and repair the wiring: . from the FULLY CLOSED signal of the BMC2 (1HA2) to the bleed pressure-regulator valve (4001HA) . from pin A/5 of the bleed pressure-regulator valve (4001HA) to the first terminal block (Ref. ASM 36-11/02).
B. After the subsequent flight, make sure that the fault does not continue.
1
-EFF : ALL
-∞∞36-11-00∞∞∞∞∞∞∞∞∞∞Page A289
--Feb 01/05R ---CES -
Amber XX on the Lower ECAM DU Replace the Position Indication of the Bleed Pressure-Regulator Valve of the Engine 2
1. Possible Causes
_______________
-BMC-2 (1HA2)
2. Job Set-up Information
______________________
A. Referenced Information
-------------------------------------------------------------------------------REFERENCE DESIGNATION -------------------------------------------------------------------------------
AMM 36-11-00-740-001 BITE Test of the BMC 1(2)
AMM 36-11-34-000-001 Removal of the BMC (1HA1, 1HA2)
AMM 36-11-34-400-001 Installation of the BMC (1HA1, 1HA2)
TSM 36 PB 101
3. Fault Confirmation
__________________
A. Test
(1) Do the BITE test of the BMC2 (Ref. AMM TASK 36-11-00-740-001).
4. Fault Isolation
_______________
A. If the test gives a maintenance message, you can find the related trouble shooting procedure in the (Ref. TSM 36 PB 101).
(1) If there is no maintenance message:
-replace the BMC-2 (1HA2) (Ref. AMM TASK 36-11-34-000-001) and (Ref. AMM TASK 36-11-34-400-001).
B. After the subsequent flight, make sure that the fault does not continue.
1
-EFF : ALL
-∞∞36-11-00∞∞∞∞∞∞∞∞∞∞Page A290
--Feb 01/05R ---CES -
Amber XX on the Lower ECAM DU Replace the Position Indication of the HP Bleed Valve of the Engine 2
1. Possible Causes
_______________
-BMC-2 (1HA2)
2. Job Set-up Information
______________________
A. Referenced Information
-------------------------------------------------------------------------------REFERENCE DESIGNATION -------------------------------------------------------------------------------
AMM 36-11-00-740-001 BITE Test of the BMC 1(2)
AMM 36-11-34-000-001 Removal of the BMC (1HA1, 1HA2)
AMM 36-11-34-400-001 Installation of the BMC (1HA1, 1HA2)
TSM 36 PB 101
3. Fault Confirmation
__________________
A. Test
(1) Do the BITE test of the BMC2 (Ref. AMM TASK 36-11-00-740-001).
4. Fault Isolation
_______________
A. If the test gives a maintenance message, you can find the related trouble shooting procedure in the (Ref. TSM 36 PB 101).
(1) If there is no maintenance message:
-replace the BMC-2 (1HA2) (Ref. AMM TASK 36-11-34-000-001) and (Ref. AMM TASK 36-11-34-400-001).
B. After the subsequent flight, make sure that the fault does not continue.
1
-EFF : ALL
-∞∞36-11-00∞∞∞∞∞∞∞∞∞∞Page A291
中国航空网 www.aero.cn
航空翻译 www.aviation.cn
本文链接地址:A320 Trouble Shooting Manual 排故手册 PNEUMATIC(83)