3. Fault Confirmation
__________________
 A. Test
 (1) Do the BITE test of the BMC 2 (Ref. AMM TASK 36-11-00-740-001).
 4. Fault Isolation
_______________
 A. If the BITE test gives no maintenance message:
 -no maintenance is necessary.
 (1)
 If the BITE test gives the class 3 maintenance message:
 TEMP SENSOR 6HA2
 -replace the SENSOR-EXCHANGER OUT TEMP, ENG 2 (6HA2) (Ref. AMM TASK 36-11-17-000-001) and (Ref. AMM TASK 36-11-17-400-001).
 (2)
 If the BITE test gives the class 3 maintenance message:
 HP BLEED-V 4000HA2
 -replace the VALVE-HP BLEED (4000HA) of the engine 2 (Ref. AMM TASK 36-11-51-000-042) and (Ref. AMM TASK 36-11-51-400-042).
 B. After the subsequent flight, make sure that the fault does not continue.
 1
 -EFF : ALL
-∞∞36-11-00∞∞∞∞∞∞∞∞∞∞Page A260
 --Feb 01/05R ---CES -
 Loss of the Bleed Temperature Monitoring of the Engine 2
 1. Possible Causes
_______________
 -SENSOR-EXCHANGER OUT TEMP, ENG 2 (6HA2)
 -BMC-2 (1HA2)
 2. Job Set-up Information
______________________
 A. Referenced Information
 -------------------------------------------------------------------------------REFERENCE DESIGNATION -------------------------------------------------------------------------------
AMM 36-11-00-740-001 BITE Test of the BMC 1(2) AMM 36-11-17-000-001 Removal of the Heat-Exchanger Outlet-Temperature Sensor 6HA1(6HA2) AMM 36-11-17-400-001 Installation of the Heat-Exchanger Outlet-Temperature
 Sensor 6HA1(6HA2) AMM 36-11-34-000-001 Removal of the BMC (1HA1, 1HA2) AMM 36-11-34-400-001 Installation of the BMC (1HA1, 1HA2) TSM 36 PB 101
 3. Fault Confirmation
__________________
 A. Test
 (1) Do the BITE test of the BMC2 (Ref. AMM TASK 36-11-00-740-001).
 4. Fault Isolation
_______________
 A. If the test gives a maintenance message, you can find the related trouble shooting procedure in the (Ref. TSM 36 PB 101).
 (1) If there is no maintenance message:
 -replace the SENSOR-EXCHANGER OUT TEMP, ENG 2 (6HA2) (Ref. AMM TASK 36-11-17-000-001) and (Ref. AMM TASK 36-11-17-400-001).
 (a) If the fault continues:
 -replace the BMC-2 (1HA2) (Ref. AMM TASK 36-11-34-000-001) and (Ref. AMM TASK 36-11-34-400-001).
 B. After the subsequent flight, make sure that the fault does not continue.
 1
 -EFF : ALL
-∞∞36-11-00∞∞∞∞∞∞∞∞∞∞Page A261
--Feb 01/05R ---CES -
 Small Variation of the Bleed Pressure Indication
 1. Possible Causes_______________
 2. Job Set-up Information______________________ Not Applicable
 3. Fault Confirmation__________________
 A. Test
 Not applicable, it is not a fault.
 4. Fault Isolation_______________
 A. No maintenance action is required.
 1
 -EFF : ALL
-∞∞36-11-00∞∞∞∞∞∞∞∞∞∞Page A262
 --Feb 01/05R ---CES -
 Variation of the Bleed Pressure Indication for the Engine 1
 1. Possible Causes_______________
 -SOLENOID-BLEED PRESS REG V CTL, ENG 1 (10HA1)
 -sense line
 2. Job Set-up Information______________________
 A. Referenced Information
 -------------------------------------------------------------------------------
REFERENCE  DESIGNATION
 -------------------------------------------------------------------------------
AMM 36-11-00-720-007  Functional Test of the Sense Lines Upstream of the Bleed Pressure Regulator Valve (4001HA) and Connected to the Control Solenoid (10HA1,10HA2)
 AMM 36-11-00-740-001  BITE Test of the BMC 1(2)
 AMM 36-11-55-000-001  Removal of the Bleed-Pressure-Regulator Valve Control-Solenoid (10HA1,10HA2)
 AMM 36-11-55-400-001  Installation of the Bleed-Pressure-Regulator Valve Control-Solenoid (10HA1,10HA2)
 3. Fault Confirmation__________________
 
中国航空网 www.aero.cn
航空翻译 www.aviation.cn
本文链接地址:A320 Trouble Shooting Manual 排故手册 PNEUMATIC(74)