-∞∞36-11-00∞∞∞∞∞∞∞∞∞∞Page A237
--Feb 01/05R ---CES -
Low Bleed Pressure of the Engine 1 in Descent/Taxi
1. Possible Causes
_______________
-VALVE-HP BLEED (4000HA)
-sense line
2. Job Set-up Information
______________________
A. Referenced Information
-------------------------------------------------------------------------------REFERENCE DESIGNATION
-------------------------------------------------------------------------------
AMM 36-11-00-740-001 BITE Test of the BMC 1(2)
AMM 36-11-51-000-040 Removal of the High Pressure Bleed Valve (4000HA)
AMM 36-11-51-400-040 Installation of the High Pressure Bleed Valve
(4000HA) TSM 36 PB 101
3. Fault Confirmation
__________________
A. Test
(1) Do the BITE test of the BMC1 (Ref. AMM TASK 36-11-00-740-001).
4. Fault Isolation
_______________
A. If the test gives a maintenance message, you can find the related trouble shooting procedure in the (Ref. TSM 36 PB 101).
(1) If there is no maintenance message:
-replace the VALVE-HP BLEED (4000HA) (Ref. AMM TASK 36-11-51-000-040) and (Ref. AMM TASK 36-11-51-400-040).
(a) If the fault continues:
-replace the sense line between the bleed pressure-regulator valve control-solenoid (10HA1) and the bleed pressure-regulator valve (4001HA).
B. After the subsequent flight, make sure that the fault does not continue.
1
-EFF : ALL
-∞∞36-11-00∞∞∞∞∞∞∞∞∞∞Page A238
--Feb 01/05R ---CES -
Loss of the Bleed Pressure Monitoring of the Engine 1
1. Possible Causes
_______________
-XDCR-BLEED REGULATED PRESS, ENG 1 (8HA1)
-BMC-1 (1HA1)
2. Job Set-up Information
______________________
A. Referenced Information
-------------------------------------------------------------------------------REFERENCE DESIGNATION -------------------------------------------------------------------------------
AMM 36-11-00-740-001 BITE Test of the BMC 1(2) AMM 36-11-16-000-001 Removal of the Bleed Regulated Pressure Transducer (8HA1,8HA2) AMM 36-11-16-400-001 Installation of the Bleed Regulated Pressure
Transducer (8HA1,8HA2) AMM 36-11-34-000-001 Removal of the BMC (1HA1, 1HA2) AMM 36-11-34-400-001 Installation of the BMC (1HA1, 1HA2) TSM 36 PB 101
3. Fault Confirmation
__________________
A. Test
(1) Do the BITE test of the BMC1 (Ref. AMM TASK 36-11-00-740-001).
4. Fault Isolation
_______________
A. If the test gives a maintenance message, you can find the related trouble shooting procedure in the (Ref. TSM 36 PB 101).
(1) If there is no maintenance message:
-replace the XDCR-BLEED REGULATED PRESS, ENG 1 (8HA1) (Ref. AMM TASK 36-11-16-000-001) and (Ref. AMM TASK 36-11-16-400-001).
(a) If the fault continues:
-replace the BMC-1 (1HA1) (Ref. AMM TASK 36-11-34-000-001) and (Ref. AMM TASK 36-11-34-400-001).
B. After the subsequent flight, make sure that the fault does not continue.
1
-EFF : ALL
-∞∞36-11-00∞∞∞∞∞∞∞∞∞∞Page A239
--Feb 01/05R ---CES -
High Bleed Pressure of the Engine 2 in Climb
1. Possible Causes
_______________
-VALVE-BLEED PRESS REG (4001HA)
-VALVE-OVERPRESSURE, ENG 2 (5HA2)
2. Job Set-up Information
______________________
A. Referenced Information
-------------------------------------------------------------------------------REFERENCE DESIGNATION -------------------------------------------------------------------------------
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