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时间:2011-03-28 23:25来源:蓝天飞行翻译 作者:航空
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 A. Test
 (1) Do the BITE test of the BMC1 (Ref. AMM TASK 36-11-00-740-001).
 4. Fault Isolation_______________
 A. If the test gives a maintenance message, you can find the related trouble shooting procedure in the applicable Page Block 101.
 (1) If there is no maintenance message:
 -do a check of the sense line unions at the bleed pressure-regulator valve of the engine 1 (4001HA) and the related control solenoid (10HA1).
 (a)
 If the unions are loose:

 -tighten these unions again (specified torque value is 1.6 m.daN).

 (b)
 If the unions are correct:


 -do the functional test of the upstream sense line between the bleed pressure-regulator valve (4001HA) and the control solenoid (10HA1) (Ref. AMM TASK 36-11-00-720-007).
 1
 -EFF : ALL


-∞∞36-11-00∞∞∞∞∞∞∞∞∞∞Page A263

 --Feb 01/05R ---CES -

 

 1 If the pressure drop is high:
_
 -replace the sense line. 2 If the pressure drop is slow or stays constant:
_
 -do a check for leaks on the sense line at the engine/pylon connection. To do this, manually move the sense line.
 a If the pressure drop is high:
_
 -replace the sense line. b If the pressure drop is not high:
_
 -replace the SOLENOID-BLEED PRESS REG V CTL, ENG 1 (10HA1) (Ref. AMM TASK 36-11-55-000-001) and (Ref. AMM TASK 36-11-55-400-001).
 B. After the subsequent flight, make sure that the fault does not continue.
 1
 -EFF : ALL


-∞∞36-11-00∞∞∞∞∞∞∞∞∞∞Page A264
 --Feb 01/05R ---CES -


 Variation of the Bleed Pressure Indication for the Engine 2
 1. Possible Causes_______________
 -SOLENOID-BLEED PRESS REG V CTL, ENG 2 (10HA2)
 -sense line
 2. Job Set-up Information______________________
 A. Referenced Information
 -------------------------------------------------------------------------------
REFERENCE  DESIGNATION
 -------------------------------------------------------------------------------
AMM 36-11-00-720-007  Functional Test of the Sense Lines Upstream of the Bleed Pressure Regulator Valve (4001HA) and Connected to the Control Solenoid (10HA1,10HA2)
 AMM 36-11-00-740-001  BITE Test of the BMC 1(2)
 AMM 36-11-55-000-001  Removal of the Bleed-Pressure-Regulator Valve Control-Solenoid (10HA1,10HA2)
 AMM 36-11-55-400-001  Installation of the Bleed-Pressure-Regulator Valve Control-Solenoid (10HA1,10HA2)
 TSM 36 PB 101
 3. Fault Confirmation__________________
 A. Test
 (1) Do the BITE test of the BMC2 (Ref. AMM TASK 36-11-00-740-001).
 4. Fault Isolation_______________
 A. If the test gives a maintenance message, you can find the related trouble shooting procedure in the (Ref. TSM 36 PB 101).
 (1) If there is no maintenance message:
 -do a check of the sense line unions at the bleed pressure-regulator valve of the engine 2 (4001HA) and the related control solenoid (10HA2).
 (a)
 If the unions are loose:

 -tighten these unions again (specified torque value is 1.6 m.daN).

 (b)
 If the unions are correct:


 -do the functional test of the upstream sense line between the bleed pressure-regulator valve (4001HA) and the control solenoid (10HA2) (Ref. AMM TASK 36-11-00-720-007).
 1
 -EFF : ALL


-∞∞36-11-00∞∞∞∞∞∞∞∞∞∞Page A265

 --Feb 01/05R ---CES -

 

 1 If the pressure drop is high:
_
 -replace the sense line. 2 If the pressure drop is slow or stays constant:
_
 -do a check for leaks on the sense line at the engine/pylon connection. To do this, manually move the sense line.
 a If the pressure drop is high:
_
 -replace the sense line. b If the pressure drop is not high:
_
 -replace the SOLENOID-BLEED PRESS REG V CTL, ENG 2 (10HA2) (Ref. AMM TASK 36-11-55-000-001) and (Ref. AMM TASK 36-11-55-400-001).
 B. After the subsequent flight, make sure that the fault does not continue.
 1
 -EFF : ALL


-∞∞36-11-00∞∞∞∞∞∞∞∞∞∞Page A266
 --Feb 01/05R ---CES -


 High Variation of the Bleed Pressure Indication for the Engine 1
 1. Possible Causes
_______________
 -SOLENOID-BLEED PRESS REG V CTL, ENG 1 (10HA1)
 
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