-tighten these unions again (specified torque value is 1.6 m.daN).
(b)
If the unions are correct:
-do the functional test of the upstream sense line between the bleed pressure-regulator valve (4001HA) and the control solenoid (10HA1) (Ref. AMM TASK 36-11-00-720-007).
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1 If the pressure drop is high:
_
-replace the sense line. 2 If the pressure drop is slow or stays constant:
_
-do a check for leaks on the sense line at the engine/pylon connection. To do this, manually move the sense line.
a If the pressure drop is high:
_
-replace the sense line. b If the pressure drop is not high:
_
-replace the SOLENOID-BLEED PRESS REG V CTL, ENG 1 (10HA1) (Ref. AMM TASK 36-11-55-000-001) and (Ref. AMM TASK 36-11-55-400-001).
B. After the subsequent flight, make sure that the fault does not continue.
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-∞∞36-11-00∞∞∞∞∞∞∞∞∞∞Page A264
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Variation of the Bleed Pressure Indication for the Engine 2
1. Possible Causes_______________
-SOLENOID-BLEED PRESS REG V CTL, ENG 2 (10HA2)
-sense line
2. Job Set-up Information______________________
A. Referenced Information
-------------------------------------------------------------------------------
REFERENCE DESIGNATION
-------------------------------------------------------------------------------
AMM 36-11-00-720-007 Functional Test of the Sense Lines Upstream of the Bleed Pressure Regulator Valve (4001HA) and Connected to the Control Solenoid (10HA1,10HA2)
AMM 36-11-00-740-001 BITE Test of the BMC 1(2)
AMM 36-11-55-000-001 Removal of the Bleed-Pressure-Regulator Valve Control-Solenoid (10HA1,10HA2)
AMM 36-11-55-400-001 Installation of the Bleed-Pressure-Regulator Valve Control-Solenoid (10HA1,10HA2)
TSM 36 PB 101
3. Fault Confirmation__________________
A. Test
(1) Do the BITE test of the BMC2 (Ref. AMM TASK 36-11-00-740-001).
4. Fault Isolation_______________
A. If the test gives a maintenance message, you can find the related trouble shooting procedure in the (Ref. TSM 36 PB 101).
(1) If there is no maintenance message:
-do a check of the sense line unions at the bleed pressure-regulator valve of the engine 2 (4001HA) and the related control solenoid (10HA2).
(a)
If the unions are loose:
-tighten these unions again (specified torque value is 1.6 m.daN).
(b)
If the unions are correct:
-do the functional test of the upstream sense line between the bleed pressure-regulator valve (4001HA) and the control solenoid (10HA2) (Ref. AMM TASK 36-11-00-720-007).
1
-EFF : ALL
-∞∞36-11-00∞∞∞∞∞∞∞∞∞∞Page A265
--Feb 01/05R ---CES -
1 If the pressure drop is high:
_
-replace the sense line. 2 If the pressure drop is slow or stays constant:
_
-do a check for leaks on the sense line at the engine/pylon connection. To do this, manually move the sense line.
a If the pressure drop is high:
_
-replace the sense line. b If the pressure drop is not high:
_
-replace the SOLENOID-BLEED PRESS REG V CTL, ENG 2 (10HA2) (Ref. AMM TASK 36-11-55-000-001) and (Ref. AMM TASK 36-11-55-400-001).
B. After the subsequent flight, make sure that the fault does not continue.
1
-EFF : ALL
-∞∞36-11-00∞∞∞∞∞∞∞∞∞∞Page A266
--Feb 01/05R ---CES -
High Variation of the Bleed Pressure Indication for the Engine 1
1. Possible Causes
_______________
-SOLENOID-BLEED PRESS REG V CTL, ENG 1 (10HA1)
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