2 If the pressure decreases to "0" psig in less than 20 seconds:
_
-do an internal leakage check of the bleed pressure regulator valve control solenoid
-disconnect the sense line at the bleed pressure regulator valve control solenoid. Put a blanking cap on the sense line
-pressurize the sense line to 30 psi (2.0684 bar) then close the shut off valve of the pressure source.
a If the pressure decreases:
_ -repair or replace the sense line.
b If the pressure stays constant:
_
-replace the SOLENOID-BLEED PRESS REG V CTL, ENG 2 (10HA2) (Ref. AMM TASK 36-11-55-000-001) and (Ref. AMM TASK 36-11-55-400-001).
(3) If the fault continues:
-
do a check of the correct indication of the bleed regulated pressure transducer (8HA2)
- on the AIR control panel 30VU, push the APU BLEED pusbutton switch and set the X-BLEED selector switch to OPEN
-
do a check on the ECAM BLEED page of the pressure indications of the two systems.
1
-EFF : ALL
-∞∞36-11-00∞∞∞∞∞∞∞∞∞∞Page 221
--Feb 01/05R ---CES -
(a) If the pressure indication of the defective system is 8 psi (0.5515 bar) minimum less than that of the opposite system:
-replace the XDCR-BLEED REGULATED PRESS, ENG 2 (8HA2) (Ref. AMM TASK 36-11-16-000-001) and (Ref. AMM TASK 36-11-16-400-001).
B. After the subsequent flight, make sure that the fault does not continue.
1
-EFF : ALL
-∞∞36-11-00∞∞∞∞∞∞∞∞∞∞Page 222
--Feb 01/05R ---CES -
Overpressure Valve of the Engine 1 Blocked in the not Fully Open Position
1. Possible Causes
_______________
-VALVE-OVERPRESSURE, ENG 1 (5HA1)
-BMC-1 (1HA1)
-wiring from the BMC1 (1HA1) to the overpressure valve (5HA1)
2. Job Set-up Information
______________________
A. Referenced Information
-------------------------------------------------------------------------------REFERENCE DESIGNATION
-------------------------------------------------------------------------------
AMM 36-11-34-000-001 Removal of the BMC (1HA1, 1HA2)
AMM 36-11-34-400-001 Installation of the BMC (1HA1, 1HA2)
AMM 36-11-53-000-001 Removal of the Overpressure Valve (5HA1,5HA2)
AMM 36-11-53-400-001 Installation of the Overpressure Valve (5HA1,5HA2)
ASM 36-11/01
3. Fault Confirmation
__________________
A. Test
(1) Not applicable, the fault is evident.
4. Fault Isolation
_______________
R **ON A/C 001-049, 051-099, 101-105, 151-199, 201-228, 301-302,
A. If the fault symptom is identified by the maintenance message: OVERPRESS-V-5HA1
-replace the VALVE-OVERPRESSURE, ENG 1 (5HA1) (Ref. AMM TASK 36-11-53-000-001) and (Ref. AMM TASK 36-11-53-400-001).
(1)
If the fault continues:
-replace the BMC-1 (1HA1) (Ref. AMM TASK 36-11-34-000-001) and (Ref. AMM TASK 36-11-34-400-001).
(2)
If the fault continues:
-do a check and repair the wiring from the BMC1 (1HA1) to the overpressure valve (5HA1), pin AA/10A to pin A/1 (Ref. ASM 36-11/01).
1 -EFF : ALL
-∞∞36-11-00∞∞∞∞∞∞∞∞∞∞Page 223
--May 01/05 ---CES -R **ON A/C 106-149, 229-299, 303-399, 401-499,
A. If the fault symptom is identified by the maintenance message: OVPRESS-V-5HA1
-replace the VALVE-OVERPRESSURE, ENG 1 (5HA1) (Ref. AMM TASK 36-11-53-000-001) and (Ref. AMM TASK 36-11-53-400-001).
(1)
If the fault continues:
-replace the BMC-1 (1HA1) (Ref. AMM TASK 36-11-34-000-001) and (Ref. AMM TASK 36-11-34-400-001).
(2)
If the fault continues:
-do a check and repair the wiring from the BMC1 (1HA1) to the overpressure valve (5HA1), pin AA/10A to pin A/1 (Ref. ASM 36-11/01).
**ON A/C ALL
B. After the subsequent flight, make sure that the fault does not continue.
1 -EFF : ALL
-∞∞36-11-00∞∞∞∞∞∞∞∞∞∞Page 224
--Aug 01/05 ---CES - Overpressure Valve of the Engine 2 Blocked in the not Fully Open Position
1. Possible Causes
_______________
-VALVE-OVERPRESSURE, ENG 2 (5HA2)
-BMC-2 (1HA2)
-wiring from the BMC2 (1HA2) to the overpressure valve (5HA2)
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