A. If the test gives a maintenance message, you can find the related trouble shooting procedure in the (Ref. TSM 36 PB 101).
 (1) If there is no maintenance message:
 -replace the BMC-1 (1HA1) (Ref. AMM TASK 36-11-34-000-001) and (Ref. AMM TASK 36-11-34-400-001).
 B. After the subsequent flight, make sure that the fault does not continue.
 1
 -EFF : ALL
-∞∞36-11-00∞∞∞∞∞∞∞∞∞∞Page A282
 --Feb 01/05R ---CES -
 Amber XX on the Lower ECAM DU Replace the Position Indication of the HP Bleed Valve of the Engine 1
 1. Possible Causes
_______________
 -BMC-1 (1HA1)
 2. Job Set-up Information
______________________
 A. Referenced Information
 -------------------------------------------------------------------------------REFERENCE DESIGNATION -------------------------------------------------------------------------------
AMM 36-11-00-740-001 BITE Test of the BMC 1(2)
 AMM 36-11-34-000-001 Removal of the BMC (1HA1, 1HA2)
 AMM 36-11-34-400-001 Installation of the BMC (1HA1, 1HA2)
 TSM 36 PB 101
3. Fault Confirmation
__________________
 A. Test
 (1) Do the BITE test of the BMC1 (Ref. AMM TASK 36-11-00-740-001).
 4. Fault Isolation
_______________
 A. If the test gives a maintenance message, you can find the related trouble shooting procedure in the (Ref. TSM 36 PB 101).
 (1) If there is no maintenance message:
 -replace the BMC-1 (1HA1) (Ref. AMM TASK 36-11-34-000-001) and (Ref. AMM TASK 36-11-34-400-001).
 B. After the subsequent flight, make sure that the fault does not continue.
 1
 -EFF : ALL
-∞∞36-11-00∞∞∞∞∞∞∞∞∞∞Page A283
 --Feb 01/05R ---CES -
 The Bleed Pressure-Regulator Valve of the Engine 2 is Shown Open Amber on the Lower ECAM DU
 1. Possible Causes_______________
 -VALVE-BLEED PRESS REG (4001HA)
 -SOLENOID-BLEED PRESS REG V CTL, ENG 2 (10HA2)
 -XDCR-BLEED TRANSFER PRESS, ENG 2 (7HA2)
 -wiring
 2. Job Set-up Information______________________
 A. Referenced Information
 -------------------------------------------------------------------------------
REFERENCE  DESIGNATION
 -------------------------------------------------------------------------------
AMM 36-11-00-740-001  BITE Test of the BMC 1(2)
 AMM 36-11-15-000-001  Removal of the Bleed Transferred Pressure Transducer (7HA1,7HA2)
 AMM 36-11-15-400-001  Installation of the Bleed Transferred Pressure Transducer (7HA1,7HA2)
 AMM 36-11-52-000-040  Removal of the Bleed Pressure-Regulator Valve (4001HA)
 AMM 36-11-52-400-040  Installation of the Bleed Pressure-Regulator Valve (4001HA)
 AMM 36-11-55-000-001  Removal of the Bleed-Pressure-Regulator Valve Control-Solenoid (10HA1,10HA2)
 AMM 36-11-55-400-001  Installation of the Bleed-Pressure-Regulator Valve Control-Solenoid (10HA1,10HA2)
 ASM 36-11/02
 TSM 36 PB 101
 3. Fault Confirmation__________________
 A. Test
 (1) Do the BITE test of the BMC2 (Ref. AMM TASK 36-11-00-740-001).
 1
 -EFF : ALL
-∞∞36-11-00∞∞∞∞∞∞∞∞∞∞Page A284
 --Feb 01/05R ---CES -
 4. Fault Isolation
_______________
 A. If the test gives a maintenance message, you can find the related trouble shooting procedure in the (Ref. TSM 36 PB 101).
 (1) If there is no maintenance message:
 -replace the VALVE-BLEED PRESS REG (4001HA) (Ref. AMM TASK 36-11-52-000-040) and (Ref. AMM TASK 36-11-52-400-040).
 (a) If the fault continues:
 -replace the SOLENOID-BLEED PRESS REG V CTL, ENG 2 (10HA2) (Ref. AMM TASK 36-11-55-000-001) and (Ref. AMM TASK 36-11-55-400-001).
 1_ If the fault continues: 
 - replace the XDCR-BLEED TRANSFER PRESS, ENG 2 (7HA2) (Ref. 
 AMM TASK 36-11-15-000-001) and (Ref. AMM TASK 36-11-15-400- 
001).
 a If the fault continues:
_
 -do a check and repair the wiring: . from the FULLY CLOSED signal of the BMC2 (1HA2) to the bleed pressure-regulator valve (4001HA) . from pin A/3 of the bleed pressure-regulator valve (4001HA) to the first terminal block (Ref. ASM 36-11/02).
 B. After the subsequent flight, make sure that the fault does not continue.
 1
 
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