R (b) If all the circuit breakers are closed:
R - stop the engine 2 (Ref. AMM TASK 71-00-00-710-043)
R - de-energize the aircraft electrical network from the external
R power (Ref. AMM TASK 24-41-00-862-002) and do the procedure
R that follows.
R C. Do a check of the AC/DC main power center 120VU:
R - open the AC/DC main power center 120VU and do a check of the wiring for
R a short circuit or a short to ground between downstream of the GLC 2
R (load side) and the loads (Ref. ASM 24-51/03).
R (1) If the wiring is not correct:
R - repair or replace as necessary.
R (2) If the wiring is correct:
R - do a check of the feeders for a short to ground, a short circuit or
R a related defective equipement between the pins R, M, G, P, L, H,
R N, K and J of the GLC 2 and the load side (Ref. ASM 24-51/03).
「一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一1 EFF : 401-499, ∞∞24-20-00∞∞∞∞∞∞∞∞∞∞Page B297
Aug 01/05 CES
R (a) If there is a short to ground:
R - repair or replace as necessary.
R (b) If there is no short to ground:
R - energize the aircraft electrical network from the external
R power (Ref. AMM TASK 24-41-00-861-002)
R - start the engine 2 only (Ref. AMM TASK 71-00-00-710-043) and
R close one by one the circuit breakers until the warning GEN 2
R OVERLOAD is shown. Repair the wiring or the component of the
R defective circuit.
R D. Do this test to make sure that the failure is repaired:
R (1) Make sure that the circuit breakers are closed (if the circuit
R breakers are not closed, close them).
R (2) Energize the aircraft electrical circuit from the external power
R (Ref. AMM TASK 24-41-00-861-002).
R (3) On the ELEC panel 35VU, make sure that the ELEC/GALLEY pushbutton
R switch is pushed.
R (4) Start the engine 2 (Ref. AMM TASK 71-00-00-710-003).
R (5) After five minutes, make sure that, on the upper ECAM DU, the warning
R GEN 2 OVERLOAD is not shown.
R (6) Stop the engine 2 (Ref. AMM TASK 71-00-00-710-028).
R 5. Close-up________
R A. Put the aircraft back to its initial configuration.
R (1) De-energize the aircraft electrical circuits from the external power
R (Ref. AMM TASK 24-41-00-862-002).
R TASK 24-20-00-810-920 R Failure of the BTC 1 Status Sense-Circuit R 1. Possible Causes
_______________
R - GCU-1 (1XU1) R - BTC-1 (11XU1) R - wiring
R 2. Job Set-up Information
______________________
R A. Referenced Information
R -------------------------------------------------------------------------------R REFERENCE DESIGNATION R -------------------------------------------------------------------------------
R AMM 24-22-34-000-001 R AMM 24-22-34-400-001 R AMM 24-22-55-000-001 R AMM 24-22-55-400-002 R R AMM 24-41-00-740-002 R ASM 24-22/02
R 3. Fault Confirmation
__________________
R A. Test
Removal of the GCU-1(2) (1XU1, 1XU2)
Installation of the GCU-1(2) (1XU1, 1XU2)
Removal of the Contactors (9XU1, 9XU2, 11XU1, 11XU2)
Installation of the Contactors (9XU1, 9XU2, 11XU1,
11XU2)
Operational Check of GAPCU via CFDS
R (1) Do the BITE test of the GAPCU (Ref. AMM TASK 24-41-00-740-002).
R NOTE : If the CFDS message PB BUS TIE (10XU) / BTC1 (11XU1) / GCU1
____ R (1XU1) comes into view when the flight crew or the maintenance R personnel puts the BUS TIE pushbutton switch (10XU) in the R released or OFF position the trouble shooting is not R necessary. This can occur during an electrical system test or R during trouble shooting. R If the flight crew or the maintenance personnel did not R operate the BUS TIE pushbutton switch and this CFDS message R comes into view, do the trouble shooting procedure that R follows.
R (a) If the BITE test gives the message TEST FAILED: R - do the trouble shooting given in Para 4.A.
R (b) If the BITE test gives the message TEST PASSED: R - do the trouble shooting given in Para 4.B.
「一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一1 EFF : 401-499, ∞∞24-20-00∞∞∞∞∞∞∞∞∞∞Page B299
Aug 01/05 CES
R 4. Fault Isolation_______________
R A. If the BITE test gives the message TEST FAILED:
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