- do a check of the current value with an ammeter (Ref. TASK 24-38-00-810-843).
(2) If the value of the discharge current is less than 1 ampere:
- replace the BAT-1 (2PB1), (Ref. AMM TASK 24-38-51-000-001) and (Ref. AMM TASK 24-38-51-400-001)
- wait at least 15 minutes and do the BITE test of the BCL1 given in Para. 4.C.
(a) If the BITE test gives the maintenance message CHECK HOT BUS 1 POWER CONSUMPTION:
- replace the BCL-1 (1PB1), (Ref. AMM TASK 24-38-34-000-001) and (Ref. AMM TASK 24-38-34-400-001).
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(b) If the BITE test gives the maintenance message TEST OK:
- make sure that after the subsequent flight, the maintenance message CHECK HOT BUS 1 POWER COSUMPTION does not appear.
1 If the maintenance message CHECK HOT BUS 1 POWER CONSUMPTION
_
appear:
- replace the BCL-1 (1PB1), (Ref. AMM TASK 24-38-34-000-001) and (Ref. AMM TASK 24-38-34-400-001).
B. Preparation for the test
(1) Energize the aircraft electrical circuits
(Ref. AMM TASK 24-41-00-861-002).
C. Do this test to make sure that the system operates correctly
NOTE : Wait at least 15 minutes and do this BITE test of the BCL1.
____
-------------------------------------------------------------------------------ACTION RESULT -------------------------------------------------------------------------------
On the ELEC panel 35VU:
- push the BAT 1 pushbutton switch.
1. On the center pedestal, on the MCDU:
- push the line key adjacent to the BCL indication.
2. On the MCDU:
- push the line key adjacent to the TEST indication.
5. Close-up
________On the ELEC panel 35VU:
- the OFF legend of the BAT 1 pushbutton switch goes off.
On the MCDU:
- the BCL page comes into view.
On the MCDU, on the BCL/TEST page:
- the TEST OK message comes into view.
A. Put the aircraft back to its initial configuration.
R (1) On the MCDU, push the line key adjacent to the RETURN indication until the MCDU MENU comes into view.
R R (2) Fully decrease the brightness of the MCDU screen (display off).
(3) De-energize the aircraft electrical circuits (Ref. AMM TASK 24-41-00-862-002).
TASK 24-38-00-810-835
Abnormal Power Consumption on the 28VDC HOT BUS (702PP)
1. Possible Causes
_______________
- BAT-2 (2PB2)
- BCL-2 (1PB2)
2. Job Set-up Information
______________________
A. Referenced Information
-------------------------------------------------------------------------------REFERENCE DESIGNATION -------------------------------------------------------------------------------
24-38-00-810-838 Incorrect Discharge of the Battery 2 AMM 24-38-34-000-001 Removal of the Battery Charge Limiter (BCL) (1PB1, 1PB2) AMM 24-38-34-400-001 Installation of the Battery Charge Limiter (BCL)
(1PB1, 1PB2) AMM 24-38-51-000-001 Removal of the Batteries (2PB1, 2PB2) AMM 24-38-51-400-001 Installation of the Batteries (2PB1, 2PB2) AMM 24-41-00-861-002 Energize the Aircraft Electrical Circuits from the
External Power AMM 24-41-00-862-002 De-energize the Aircraft Electrical Circuits Supplied from the External Power AMM 31-32-00-860-004 Procedure to Get Access to the SYSTEM REPORT/TEST/ELEC Page 24-38-00-991-002 Fig. 202
3. Fault Confirmation
__________________
(Ref. Fig. 202/TASK 24-38-00-991-002)
A. Job Set-Up
(1) Aircraft Maintenance Configuration
(a) Energize the aircraft electrical circuits (Ref. AMM TASK 24-41-00-861-002).
(b) On the overhead panel, on the ELEC panel 35VU, make sure that the BAT2 pushbutton switch is pushed (the OFF legend is off).
R (c) Adjust the brightness of the MCDU screen.
R (d) On the MCDU, get the SYSTEM REPORT/TEST/ELEC page (Ref. AMM TASK 31-32-00-860-004).
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BAT2 - Ammeter Installation
Figure 202/TASK 24-38-00-991-002
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