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时间:2011-03-29 09:37来源:蓝天飞行翻译 作者:航空
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 (2) If the fault continues:

 - make sure that there is 28VDC at the pin 9 of the connector 1KS2-AC (Ref. ASM 73-25/05).
 (a) If there is no 28VDC:

 - do a check and repair the wiring between the circuit breaker 4KS2 and the EIU 2 (1KS2).

 (b) If there is 28VDC:


 - do a check and repair the wiring between the pin 2 of the connector 1KS2-AC and the pin 13 of the connector 4000KS-J2.

 (3) If the fault continues:


 - replace the EIU-2 (1KS2), (Ref. AMM TASK 73-25-34-000-040) and (Ref. AMM TASK 73-25-34-400-040).
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 C. Test
 (1) Do the operational test of the Engine Interface Unit (Ref. AMM TASK 73-25-34-710-043).

 (2) Make sure that all engine 2 parameters are shown on the upper ECAM DU when you start the engine again (Ref. AMM TASK 71-00-00-710-003) or (Ref. AMM TASK 71-00-00-710-004).


 5. Close-up________
 A. Put the aircraft back to its initial configuration.
 (1) Do the EIS stop procedure (Ref. AMM TASK 31-60-00-860-002).
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 TASK 73-29-00-810-804
 No engine 1 parameters are not XX on the upper ECAM DU after an engine shutdown time on the ground of 5 minutes minimum.
 1. Possible Causes
_______________
 - EIU-1 (1KS1)

 - wiring between the ENG/MASTER CTL switch (3KC) and the EIU 1 (1KS1)

 - CTL SW - ENG/MASTER 1 (3KC)


 2. Job Set-up Information
______________________
 A. Referenced Information
 -------------------------------------------------------------------------------
REFERENCE DESIGNATION
 -------------------------------------------------------------------------------
AMM 73-25-34-000-040 Removal of the Engine Interface Unit (EIU)
 (1KS1,1KS2)
 AMM 73-25-34-400-040 Installation of the Engine Interface Unit (EIU)
 (1KS1,1KS2)
 AMM 73-25-34-710-040 Operational Test of the Engine Interface Unit

 (1KS1,1KS2)
 AMM 73-25-34-710-043 Operational Test of the Engine Interface Unit
 ASM 73-25/08

 3. Fault Confirmation
__________________
 A. Test
 (1) Make sure that the engine 1 shutdown time was of 5 minutes minimum.

 (2) Do the operational test of the Engine Interface Unit (Ref. AMM TASK 73-25-34-710-043).


 4. Fault Isolation
_______________
 A. If the test gives the maintenance message 115VU (MASTER LEVER 1SW):
 - do a check and repair the wiring between the ENG/MASTER CTL switch (3KC) and the EIU 1 (1KS1), (Ref. ASM 73-25/08).
 (1) If the fault continues:
 (a) Replace the CTL SW - ENG/MASTER 1 (3KC).

 (b) Do the operational test of the Engine Interface Unit (Ref. AMM TASK 73-25-34-710-040).


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 - replace the EIU-1 (1KS1), (Ref. AMM TASK 73-25-34-000-040) and (Ref. AMM TASK 73-25-34-400-040).
 B. If the test gives NO FAILURE message:
 - replace the EIU-1 (1KS1), (Ref. AMM TASK 73-25-34-000-040) and (Ref. AMM TASK 73-25-34-400-040).
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 TASK 73-29-00-810-805
 No engine 2 parameters are not XX on the upper ECAM DU after an engine shutdown time on the ground of 5 minutes minimum.
 1. Possible Causes
_______________
 - EIU-2 (1KS2)

 - wiring between the ENG/MASTER CTL switch (2KC) and the EIU 2 (1KS2)

 - CTL SW - ENG/MASTER 2 (2KS)


 2. Job Set-up Information
______________________
 A. Referenced Information
 -------------------------------------------------------------------------------
REFERENCE DESIGNATION
 -------------------------------------------------------------------------------
 
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