F 『
E C F M E
E E
E 56 E
E E
TASK 73-25-00-810-920
Loss of 28VDC Power Supply of the ECU on the Engine 1
1. Possible Causes
_______________
- EIU-1 (1KS1)
- ECU (4000KS)
- aircraft wiring
- C/B-ENGINE/1/FADEC A/AND EIU 1 (2KS1)
- C/B-ENGINE/ENG 1/FADEC B/AND EIU 1 (4KS1)
- harnesses J1 and J2
2. Job Set-up Information
______________________
A. Referenced Information
-------------------------------------------------------------------------------REFERENCE DESIGNATION -------------------------------------------------------------------------------
AMM 73-21-60-000-001 Removal of the Electronic Control Unit (ECU)(4000KS) AMM 73-21-60-400-001 Installation of the Electronic Control Unit (ECU)(4000KS) AMM 73-25-34-000-040 Removal of the Engine Interface Unit (EIU) (1KS1,1KS2) AMM 73-25-34-400-040 Installation of the Engine Interface Unit (EIU) (1KS1,1KS2) AMM 73-29-00-710-040 Operational Test of the FADEC on the ground (with
Engine Motoring)
ASM 73-25/05
ASM 73-25/08
3. Fault Confirmation
__________________
A. Do the operational test of the FADEC 1A on the ground (with engine motoring) (Ref. AMM TASK 73-29-00-710-040).
4. Fault Isolation
_______________
A. Table of the circuit breakers used in this procedure:
-------------------------------------------------------------------------------PANEL DESIGNATION IDENT. LOCATION -------------------------------------------------------------------------------49VU ENGINE/1/FADEC A/AND EIU 1 2KS1 A04 121VU ENGINE/ENG1/FADEC B/AND EIU 1 4KS1 R41
F 『 EEFF : ALL E ∞∞73-25-00∞∞∞∞∞∞∞∞∞∞Page A204
E E Aug 01/05 ERE ECES
E
F 『
E C F M E
E E
E 56 E E E
B. If the test gives the maintenance message EIU, ECU (CR3 DIODE):
- disconnect the connectors J1 and J2 from the ECU (4000KS) and do a check for 28VDC at pins J1/13 and J2/13 with the FADEC GND PWR pushbutton switch released (the ON legend is on) (Ref. ASM 73-25/05).
(1) If there is 28VDC:
- replace the EIU-1 (1KS1) (the most possible failure is the EIU 28V relay) (Ref. AMM TASK 73-25-34-000-040) and (Ref. AMM TASK 73-25-34-400-040)
- replace the ECU (4000KS) (the most possible failure is an ECU diode) (Ref. AMM TASK 73-21-60-000-001) and (Ref. AMM TASK 73-21-60-400-001).
(2) If there is no 28VDC:
- do a check for 28VDC at EIU 1 (1KS1) pins AC/9, 11 (Ref. ASM 73-25/05).
(a) If there is no 28VDC:
- do a check for open or short to ground at the aircraft wiring from the circuit breakers (2KS1) and (4KS1) to EIU 1 (1KS1) pins AC/9, 11.
1 If there is a short to ground:
_ - repair the above wiring.
2 If there is no short to ground:
_
- replace the defective C/B-ENGINE/1/FADEC A/AND EIU 1 (2KS1) or C/B-ENGINE/ENG 1/FADEC B/AND EIU 1 (4KS1).
(b) If there is 28VDC:
- do a check for open or short to ground at the harnesses J1 and J2 between the EIU 1 (1KS1) and the ECU (4000KS), pins AC/2, 7 to pins J1/13, J2/13. Replace the harness J1 or J2 if necessary (Ref. ASM 73-25/05).
(c) If the fault continues:
- make sure that there is no ground signal at EIU 1 (1KS1) pin AA/5B (Ref. ASM 73-25/08).
(d) If the fault continues:
- replace the EIU-1 (1KS1) (Ref. AMM TASK 73-25-34-000-040) and (Ref. AMM TASK 73-25-34-400-040).
C. Do the test given in Para. 3.A.
F 『 EEFF : ALL E ∞∞73-25-00∞∞∞∞∞∞∞∞∞∞Page A205
E E Aug 01/05 ERE
ECES
F 『
E C F M E
E E
E 56 E
E E
TASK 73-25-00-810-921
Loss of 28VDC Power Supply of the ECU on the Engine 2
1. Possible Causes
_______________
- EIU-2 (1KS2)
- ECU (4000KS)
- aircraft wiring
- C/B-ENGINE/2/FADEC A/AND EIU 2 (2KS2)
- C/B-ENGINE/ENG 2/FADEC B (4KS2)
- harnesses J1 and J2
2. Job Set-up Information
______________________
A. Referenced Information
-------------------------------------------------------------------------------REFERENCE DESIGNATION -------------------------------------------------------------------------------
中国航空网 www.aero.cn
航空翻译 www.aviation.cn
本文链接地址:A320 Trouble Shooting Manual 排故手册 发动机燃油和控制 2(68)