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时间:2011-03-29 09:37来源:蓝天飞行翻译 作者:航空
曝光台 注意防骗 网曝天猫店富美金盛家居专营店坑蒙拐骗欺诈消费者

 - do a check and repair the aircraft wiring of the output 1 bus on channel A from the ECU (4000KS) to the first terminal block (Ref. ASM 73-25/10).
 B. Do the test given in Para. 3.
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ECES  TASK 73-29-00-810-837 Loss of the Output 1 Bus of the ECU 2 Channel A

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 1. Possible Causes
_______________
 - ECU (4000KS)

 - aircraft wiring


 2. Job Set-up Information
______________________
 A. Referenced Information
 -------------------------------------------------------------------------------REFERENCE DESIGNATION -------------------------------------------------------------------------------
AMM 31-50-00-710-001 Ground Scanning of the Central Warning System AMM 73-21-60-000-001 Removal of the Electronic Control Unit (ECU)(4000KS) AMM 73-21-60-400-001 Installation of the Electronic Control Unit
 (ECU)(4000KS) ASM 73-25/10
 3. Fault Confirmation
__________________
 A. Do the operational test of the Central Warning Systems (Ref. AMM TASK 31-50-00-710-001).
 4. Fault Isolation
_______________
 A. If the test gives the maintenance message FWC1 : NO DATA FROM ECU 2A:
 - replace the ECU (4000KS), (Ref. AMM TASK 73-21-60-000-001) and (Ref. AMM TASK 73-21-60-400-001).
 (1) If the fault continues:
 - do a check and repair the aircraft wiring of the output 1 bus on channel A from the ECU (4000KS) to the first terminal block (Ref. ASM 73-25/10).
 B. Do the test given in Para. 3.
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 E 56 E E E TASK 73-29-00-810-848

 Loss of Outputs 1 and 2 on Engine 1 J3 Connector
 1. Possible Causes
_______________
 - J3 connector

 - 5CA1

 - 5CA2

 - harness J3

 - ECU (4000KS)


 2. Job Set-up Information
______________________
 A. Referenced Information
 -------------------------------------------------------------------------------REFERENCE DESIGNATION -------------------------------------------------------------------------------
AMM 73-21-60-000-001 Removal of the Electronic Control Unit (ECU)(4000KS) AMM 73-21-60-400-001 Installation of the Electronic Control Unit (ECU)(4000KS) AMM 73-29-00-710-040 Operational Test of the FADEC on the ground (with Engine Motoring) ASM 73-25/12
 3. Fault Confirmation
__________________
 A. Do the operational test of the FADEC 1A on the ground (with engine
 motoring) (Ref. AMM TASK 73-29-00-710-040).

 4. Fault Isolation
_______________
 A. If the test gives the maintenance message J3 (INSTINCT DISC):
 - do a check for loose J3 connector at the ECU 1 (Ref. ASM 73-25/12).
 (1) If the fault continues:

 - make sure that the pins are not bent and that the pins and sockets have not moved into the J3 ECU 1 connector (Ref. ASM 73-25/12).

 (2) If the fault continues:


 - do a check for open circuit in the harness J3 between the pins J3/6, 31 (Ref. ASM 73-25/12).
 (a) If the fault continues:
 - replace the 5CA1

 - replace the 5CA2

 - replace the harness J3.


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 - replace the ECU (4000KS), (Ref. AMM TASK 73-21-60-000-001) and (Ref. AMM TASK 73-21-60-400-001).
 B. Do the test given in Para. 3.A.
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 E 56 E E E TASK 73-29-00-810-849

 Loss of Outputs 1 and 2 on Engine 2 J3 Connector
 1. Possible Causes
_______________
 - J3 connector

 - 5CA1

 - 5CA2

 - harness J3

 - ECU (4000KS)


 2. Job Set-up Information
______________________
 
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