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时间:2011-03-29 09:37来源:蓝天飞行翻译 作者:航空
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 Engine Motoring) ASM 73-25/05 ASM 73-25/08
 3. Fault Confirmation
__________________
 A. Make sure that this(these) circuit breaker(s) is(are) closed:
 -------------------------------------------------------------------------------PANEL DESIGNATION IDENT. LOCATION -------------------------------------------------------------------------------
121VU ENGINE/ENG1/FADEC B/AND EIU 1 4KS1 R41
 B. Test
 (1) If the circuit breaker (4KS1) is open, refer to Para. 4.A.(2).

 (2) Do the operational test of the FADEC 1B on the ground (with engine motoring) (Ref. AMM TASK 73-29-00-710-040).


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 A. If the test gives the maintenance message EIU - 28V, ECU:
 - do a check of the status of the circuit breaker (4KS1).
 (1) If the circuit breaker is closed:
 - disconnect the connector J2 from the ECU (4000KS) and do a check for 28VDC at pin J2/13 with the FADEC GND PWR pushbutton switch released (the ON legend is on) (Ref. ASM 73-25/05).
 (a) If there is 28VDC:

 - replace the EIU-1 (1KS1) (the most possible failure is the EIU 28V relay) (Ref. AMM TASK 73-25-34-000-040) and (Ref. AMM TASK 73-25-34-400-040)

 - replace the ECU (4000KS) (the most possible failure is an ECU diode) (Ref. AMM TASK 73-21-60-000-001) and (Ref. AMM TASK 73-21-60-400-001).

 

 (b) If there is no 28VDC:


 - do a check for 28VDC at EIU 1 (1KS1) pin AC/9 (Ref. ASM 73-25/05).
 1_ If there is no 28VDC:
 - do a check for open or short to ground at the aircraft
 wiring from the circuit breaker (4KS1) to EIU 1 (1KS1) pins
 AC/9.

 a If there is a short to ground:
_ - repair the above wiring.

 b If there is no short to ground:
_ - replace the C/B-ENGINE/ENG 1/FADEC B/AND EIU 1 (4KS1).

 2 If there is 28VDC:
_

 - do a check for open or short to ground at the harness J2 between the EIU 1 (1KS1) and the ECU (4000KS), pin AC/2 to pin J2/13. Replace the harness J2 if necessary (Ref. ASM 73-25/05).
 3 If the fault continues:
_

 - make sure that there is no ground signal at EIU 1 (1KS1) pin AA/5B (Ref. ASM 73-25/08).
 (c) If the fault continues:
 - replace the EIU-1 (1KS1) (Ref. AMM TASK 73-25-34-000-040) and (Ref. AMM TASK 73-25-34-400-040).
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 - close the circuit breaker.
 (a) If the circuit breaker trips:

 - replace the EIU-1 (1KS1) (Ref. AMM TASK 73-25-34-000-040) and (Ref. AMM TASK 73-25-34-400-040)

 - replace the ECU (4000KS) (Ref. AMM TASK 73-21-60-000-001) and (Ref. AMM TASK 73-21-60-400-001).

 

 (b) If the fault continues:


 - do a check for a short to ground at the harness J2 between the EIU 1 (1KS1) and the ECU (4000KS), pin AC/2 to pin J2/13.
 1 If there is a short to ground:
_ - replace the harness J2.

 2 If there is no short to ground:
_

 - do a check for a short to ground at the aircraft wiring between EIU 1 (1KS1) pin AC/9 and the circuit breaker (4KS1).
 a If there is a short to ground:
_ - repair the above wiring.

 b If there is no short to ground:
_ - replace the C/B-ENGINE/ENG 1/FADEC B/AND EIU 1 (4KS1).

 B. Do the test given in Para. 3.B.
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 Loss of the 28VDC Power Supply of the ECU on the Engine 2
 1. Possible Causes
_______________
 - EIU-2 (1KS2)

 - ECU (4000KS)

 - aircraft wiring

 - C/B-ENGINE/ENG 2/FADEC B (4KS2)

 - harness J2


 2. Job Set-up Information
______________________
 A. Referenced Information
 -------------------------------------------------------------------------------REFERENCE DESIGNATION -------------------------------------------------------------------------------
 
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