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时间:2011-03-29 09:37来源:蓝天飞行翻译 作者:航空
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 AMM 73-25-34-000-040 Removal of the Engine Interface Unit (EIU)
 AMM 73-25-34-400-040 Installation of the Engine Interface Unit (EIU)
 AMM 73-20-00 P.Block 001 CONTROLLING

 3. Fault Confirmation
__________________
 A. Not applicable.
 4. Fault Isolation
_______________
 A. Read the scheduled maintenance report or class 3 report and check if the maintenance message P0/P12/T12, ADC, ECU is present.
 (1) If the message is present:

 - check the P0 port of the ECU for absence of blockage (Ref. AMM 73-20-00 P.Block 001).

 - check the PS12 sense line for absence of blockage or leaks (Ref. AMM TASK 72-23-00-280-002). If leaks or blockage are found tighten unions or replace the PS12 sense line (Ref. AMM TASK 72-23-00-000-040) and (Ref. AMM TASK 72-23-00-400-040).

 

 (2) If nothing is found:


 - Do a check of the Post Flight Report (PFR), of the Scheduled Maintenance Report (SMR) or class 3 Report and of the FADEC Last Leg Report for LGCIU failure.
 F 『 EEFF : ALL E ∞∞73-25-00∞∞∞∞∞∞∞∞∞∞Page A200
 E E Aug 01/05 ERE ECES


 F  『
 E  C F M  E
 E  E

 

 E 56 E E E (a) If message is present:


 - do the related trouble shooting procedure for the LGCIU.
 (b) If no message is present:
 - replace the EIU-1 (1KS1) (Ref. AMM TASK 73-25-34-000-040) and (Ref. AMM TASK 73-25-34-400-040).
 (3) If the fault repeats on the subsequent flights:
 - replace the ECU (4000KS) (Ref. AMM TASK 73-21-60-000-001) and (Ref. AMM TASK 73-21-60-400-001).
 F 『 EEFF : ALL E ∞∞73-25-00∞∞∞∞∞∞∞∞∞∞Page A201
 E E Aug 01/05 ERE
ECES


 F 『
 E C F M E
 E E
 E 56 E
 E E

 

 TASK 73-25-00-810-917
 Loss of Weight on Wheels Signal on the System 2
 1. Possible Causes
_______________
 - P0 port

 - PS12 sense line

 - LGCIU

 - EIU-2 (1KS2)

 - ECU (4000KS)


 2. Job Set-up Information
______________________
 A. Referenced Information
 -------------------------------------------------------------------------------REFERENCE DESIGNATION
 -------------------------------------------------------------------------------
AMM 72-23-00-000-040 Removal of the PS12 Line
 AMM 72-23-00-280-002 Inspection/Check of the PS12 line
 AMM 72-23-00-400-040 Installation of the PS12 Line
 AMM 73-21-60-000-001 Removal of the Electronic Control Unit (ECU)
 AMM 73-21-60-400-001 Installation of the Electronic Control Unit (ECU)
 AMM 73-25-34-000-040 Removal of the Engine Interface Unit (EIU)
 AMM 73-25-34-400-040 Installation of the Engine Interface Unit (EIU)
 AMM 73-20-00 P.Block 001 CONTROLLING

 3. Fault Confirmation
__________________
 A. Not applicable.
 4. Fault Isolation
_______________
 A. Read the scheduled maintenance report or class 3 report and check if the maintenance message P0/P12/T12, ADC, ECU is present.
 (1) If the message is present:

 - check the P0 port of the ECU for absence of blockage (Ref. AMM 73-20-00 P.Block 001).

 - check the PS12 sense line for absence of blockage or leaks (Ref. AMM TASK 72-23-00-280-002). If leaks or blockage are found tighten unions or replace the PS12 sense line (Ref. AMM TASK 72-23-00-000-040) and (Ref. AMM TASK 72-23-00-400-040).

 

 (2) If nothing is found:


 - Do a check of the Post Flight Report (PFR), of the Scheduled Maintenance Report (SMR) or class 3 Report and of the FADEC Last Leg Report for LGCIU failure.
 F 『 EEFF : ALL E ∞∞73-25-00∞∞∞∞∞∞∞∞∞∞Page A202
 E E Aug 01/05 ERE ECES


 F  『
 E  C F M  E
 E  E

 

 E 56 E E E (a) If message is present:


 - do the related trouble shooting procedure for the LGCIU.
 (b) If no message is present:
 - replace the EIU-2 (1KS2) (Ref. AMM TASK 73-25-34-000-040) and (Ref. AMM TASK 73-25-34-400-040).
 (3) If the fault repeats on the subsequent flights:
 - replace the ECU (4000KS) (Ref. AMM TASK 73-21-60-000-001) and (Ref. AMM TASK 73-21-60-400-001).
 F 『 EEFF : ALL E ∞∞73-25-00∞∞∞∞∞∞∞∞∞∞Page A203
 
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