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TASK 77-00-00-810-876
Loss of the Channel B of the FADEC on Engine 1
1. Possible Causes
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- EIU-1 (1KS1)
- ECU (4000KS)
- harness J2
- aircraft wiring
- C/B-ENGINE/ENG 1/FADEC B/AND EIU 1 (4KS1)
2. Job Set-up Information
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A. Referenced Information
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REFERENCE DESIGNATION
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AMM 71-00-00-710-006 Minimum Idle Check AMM 73-21-60-000-001 Removal of the Electronic Control Unit (ECU)(4000KS) AMM 73-21-60-400-001 Installation of the Electronic Control Unit
(ECU)(4000KS) AMM 73-25-34-000-040 Removal of the Engine Interface Unit (EIU) (1KS1,1KS2) AMM 73-25-34-400-040 Installation of the Engine Interface Unit (EIU) (1KS1,1KS2) AMM 73-29-00-710-040 Operational Test of the FADEC on the ground (with
Engine Motoring)
ASM 73-25/05
ASM 73-25/08
3. Fault Confirmation
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A. Test
(1) do the operational test of the FADEC 1B on the ground (with engine motoring) (Ref. AMM TASK 73-29-00-710-040).
4. Fault Isolation
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A. Table of the circuit breakers used in this procedure:
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PANEL DESIGNATION IDENT. LOCATION
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121VU ENGINE/ENG1/FADEC B/AND EIU 1 4KS1 R41
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B. If the fault symptom is identified by the upper ECAM warning ENG1 FADEC B FAULT and the test of the FADEC 1B gives no maintenace message:
- disconnect the connector J2 from the ECU (4000KS) and do a check for 28VDC at pin J2/13 with the FADEC GND PWR pushbutton switch released (the ON legend is on).
(1) If there is 28VDC:
- replace the ECU (4000KS) (Ref. AMM TASK 73-21-60-000-001) and (Ref. AMM TASK 73-21-60-400-001).
(2) If there is no 28VDC:
- do a check for 28VDC at EIU 1 (1KS1) pin AC/9 (Ref. ASM 73-25/05).
(a) If there is 28VDC:
- do a check for open or short to ground at the harness J2 between the EIU 1 (1KS1) and the ECU (4000KS), pin AC/2 to pin J2/13. Replace the harness J2 if necessary.
(b) If there is no 28VDC:
1_ If the fault continues:
- make sure that there is no ground signal at EIU 1 (1KS1) pin
AA/5B (Ref. ASM 73-25/08).
2_ If the fault continues:
- replace the EIU-1 (1KS1) (Ref. AMM TASK 73-25-34-000-040)
and (Ref. AMM TASK 73-25-34-400-040).
- do a check for open or short to ground at the aircraft wiring between the circuit breaker (4KS1) and EIU 1 (1KS1) pin AC/9.
1 If there is a short to ground:
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- repair the above wiring. 2 If there is no short to ground:
_ - replace the C/B-ENGINE/ENG 1/FADEC B/AND EIU 1 (4KS1).
(c) Make sure that 28VDC supplies the BAT bus (Ref. ASM 73-25/05).
C. Do a minimum idle check (Ref. AMM TASK 71-00-00-710-006).
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