• 热门标签

当前位置: 主页 > 航空资料 > 机务资料 >

时间:2011-03-29 14:34来源:蓝天飞行翻译 作者:航空
曝光台 注意防骗 网曝天猫店富美金盛家居专营店坑蒙拐骗欺诈消费者

 E E Nov 01/04 ERE
ECES

 F  『
 E  C F M  E
 E  E


 E 56 E
 E E
 TASK 77-00-00-810-910


 TO/GA Inputs Invalid on Engine 1
 1. Possible Causes
_______________
 - P0 port on the ECU

 - PS12 sense line

 - LGCIU1 (5GA1)

 - EIU-1 (1KS1)

 - ECU (4000KS)

 - ADIRU 1

 - ADIRU 2


 2. Job Set-up Information
______________________
 A. Referenced Information
 -------------------------------------------------------------------------------REFERENCE DESIGNATION -------------------------------------------------------------------------------
73-25-00-810-916 Loss of Weight on Wheels Signal on the System 1 AMM 73-21-60-000-001 Removal of the Electronic Control Unit (ECU) AMM 73-21-60-400-001 Installation of the Electronic Control Unit (ECU)
 3. Fault Confirmation
__________________
 A. Test
 (1) The fault cannot be confirmed by the ground test.
 4. Fault Isolation
_______________
 A. This failure message will be set if the ECU cannot determine the take-off or go around state due to disagreement on flight/ground input signals.
 (1) If the failure message ADC1+ADC2+LGCIU1 is displayed:
 - look at the Post Flight Report or the Last Leg Report for failure message EIU, LGCIU (WOW).
 (a) If there is this message:
 - do the applicable trouble shooting procedure for this message (Ref. TASK 73-25-00-810-916).
 1 The fault may be caused by:
_
 - a blockage of the P0 port on the ECU,

 - a blockage or leakage on the PS12 sense line,

 - an LGCIU1 (5GA1) system failure,

 - an EIU-1 (1KS1) or an ECU (4000KS) internal failure.


 F 『 EEFF : ALL E ∞∞77-00-00∞∞∞∞∞∞∞∞∞∞Page A209
 E E Nov 01/04 ERE ECES

 F  『
 E  C F M  E
 E  E


 E 56 E E E (b) If there is not this message:

 - look for failure message relative to ADIRU 1 or ADIRU 2 or pitot or static probes.
 1 If there is a message:
_
 - do the applicable trouble shooting procedure.
 2 If there is no message:
_
 - replace the ECU (4000KS) (Ref. AMM TASK 73-21-60-000-001) and (Ref. AMM TASK 73-21-60-400-001).
 B. No additional maintenance action is required if the fault is not
 confirmed.

 (1) Repeat the fault isolation procedure if the fault continues.
 F 『 EEFF : ALL E ∞∞77-00-00∞∞∞∞∞∞∞∞∞∞Page A210
 E E Nov 01/04 ERE
ECES

 F  『
 E  C F M  E
 E  E


 E 56 E
 E E
 TASK 77-00-00-810-911


 TO/GA Inputs Invalid on Engine 2
 1. Possible Causes
_______________
 - P0 port on the ECU

 - PS12 sense line

 - LGCIU2 (5GA2)

 - EIU-2 (1KS2)

 - ECU (4000KS)

 - ADIRU 1

 - ADIRU 2


 2. Job Set-up Information
______________________
 A. Referenced Information
 -------------------------------------------------------------------------------REFERENCE DESIGNATION -------------------------------------------------------------------------------
73-25-00-810-917 Loss of Weight on Wheels Signal on the System 2 AMM 73-21-60-000-001 Removal of the Electronic Control Unit (ECU) AMM 73-21-60-400-001 Installation of the Electronic Control Unit (ECU)
 3. Fault Confirmation
__________________
 A. Test
 (1) The fault cannot be confirmed by the ground test.
 4. Fault Isolation
_______________
 A. This failure message will be set if the ECU cannot determine the take-off or go around state due to disagreement on flight/ground input signals.
 (1) If the failure message ADC1+ADC2+LGCIU2 is displayed:
 - look at the Post Flight Report or the Last Leg Report for failure message EIU, LGCIU (WOW).
 (a) If there is this message:
 - do the applicable trouble shooting procedure for this message (Ref. TASK 73-25-00-810-917).
 1 The fault may be caused by:
_
 - a blockage of the P0 port on the ECU,

 - a blockage or leakage on the PS12 sense line,

 - an LGCIU2 (5GA2) system failure,

 - an EIU-2 (1KS2) or an ECU (4000KS) internal failure.


 F 『 EEFF : ALL E ∞∞77-00-00∞∞∞∞∞∞∞∞∞∞Page A211
 
中国航空网 www.aero.cn
航空翻译 www.aviation.cn
本文链接地址:A320 Trouble Shooting Manual 排故手册 发动机指示(110)