- do a check of the aircraft BATTERIES (Ref. AMM TASK 24-38-00-210-001).
(1) If the fault continues:
- do a check for APU internal damage.
- do a check for contamination of the MAGNETIC-DRAIN PLUG (Ref. AMM TASK 49-91-42-200-001).
NOTE : If the MAGNETIC-DRAIN PLUG is not contaminated, continue
____
without starting the APU.
- .
- remove the end cap of the STARTER MOTOR (8KA).
- use a socket and a ratchet on the shaft of the STARTER MOTOR (8KA) to turn the APU counterclockwise (in the direction of the arrow on the housing).
- make sure that the APU rotates freely.
(a) If the APU rotates freely:
- replace the APU GENERATOR (8XS) (Ref. AMM TASK 24-23-51-000-001) and (Ref. AMM TASK 24-23-51-400-001).
1 If the fault continues:
_
- replace the STARTER MOTOR CLUTCH (Ref. AMM TASK 49-42-52-000-001) and (Ref. AMM TASK 49-42-52-400-001).
2 If the fault continues:
_
- replace the STARTER MOTOR (8KA) (Ref. AMM TASK 49-42-51-000-002) and (Ref. AMM TASK 49-42-51-400-002).
3 If the fault continues:
_
- replace the ECB (59KD) (Ref. AMM TASK 49-61-34-000-001) and (Ref. AMM TASK 49-61-34-400-001).
(b) If the APU does not rotate freely:
- replace the APU (4005KM)
B. Do the test given in para. 3.
「一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一1R EFF : 063-099, 401-499, ∞∞49-00-00∞∞∞∞∞∞∞∞∞∞Page B222
Config-1 Aug 01/05 CES
TASK 49-00-00-810-869
LOAD VALVE OPEN signal Fault (GTCP 36-300)
1. Possible Causes
_______________
- wiring
- ECB (59KD)
2. Job Set-up Information
______________________
A. Referenced Information
-------------------------------------------------------------------------------
REFERENCE DESIGNATION
-------------------------------------------------------------------------------
AMM 49-00-00-710-004 Operational Test of the APU (4005KM) (GTCP 36-300) AMM 49-61-34-000-001 Removal of the Electronic Control Box (ECB) (59KD) (GTCP 36-300) AMM 49-61-34-400-001 Installation of the Electronic Control Box (ECB) (59KD) (GTCP 36-300) ASM 21-63/02
3. Fault Confirmation
__________________
A. Do the operational test of the APU (Ref. AMM TASK 49-00-00-710-004).
4. Fault Isolation
_______________
A. If the test gives the maintenance message:
WRG: LOAD VALVE OPEN
with the LRU TROUBLE SHOOT DATA menu information:
LOAD VALVE OPEN CIRCUIT FAILURE
Fault Code Number: 138
- do a check and repair of the wiring from the ECB (59KD) AB/H8 to CONT.
- ZONE TEMP (8HK) 8HK-AA/2A (Ref. ASM 21-63/02).
(1) If the fault continues:
- replace the ECB (59KD) (Ref. AMM TASK 49-61-34-000-001) and (Ref. AMM TASK 49-61-34-400-001).
B. Do the test given in para. 3.
「一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一1R EFF : 063-099, 401-499, ∞∞49-00-00∞∞∞∞∞∞∞∞∞∞Page B223
Config-1 Aug 01/05 CES
R **ON A/C 001-003, 051-099, 401-499,
TASK 49-00-00-810-870
Clogged Oil Filter, in flight (GTCP 36-300)
1. Possible Causes
_______________
- GEN-APU (8XS)
- OIL FILTER DIFFERENTIAL PRESSURE SWITCH P9 for the lube pump filter
- OIL FILTER DIFFERENTIAL PRESSURE SWITCH P5 for the gen scavenge pump filter
- wiring
- ECB (59KD)
- AUXILIARY POWER UNIT (4005KM)
- OIL FILTER DIFFERENTIAL PRESSURE SWITCH (8070KM) for the lube pump filter
- OIL FILTER DIFFERENTIAL PRESSURE SWITCH (8071KM) for the gen scav pump filter
2. Job Set-up Information
______________________
A. Referenced Information
-------------------------------------------------------------------------------
REFERENCE DESIGNATION
-------------------------------------------------------------------------------
AMM 24-23-51-000-001 Removal of the APU Generator 8XS
AMM 24-23-51-400-001 Installation of the APU Generator 8XS
AMM 49-00-00-710-004 Operational Test of the APU (4005KM) (GTCP 36-300)
AMM 49-00-00-860-003 APU Start by External Power (GTCP 36-300)
AMM 49-00-00-860-004 APU Shutdown by External Power (GTCP 36-300)
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