F E E C F M 『EE
E E 56-5B EE
HIGHLIGHTS
__________
REVISION NO. 30 Aug 01/05
Pages which have been revised are outlined below, together with the Highlights of the Revision
CH/SE/SU C REASON FOR CHANGE EFFECTIVITY PAGES
CHAPTER 73
L.E.P.
1- 8 REVISED TO REFLECT THIS REVISION INDICATING NEW,REVISED, AND/OR DELETED PAGES
T.
OF C. REVISED TO REFLECT THIS REVISION 1-10
73-00-00 EFFECTIVITY UPDATED 1, 4, EFFECTIVITY UPDATED (THROUGHOUT THE TEXT) 106-149, 212-299, 301-399, 8-9 401-499,
73-10-00 EFFECTIVITY UPDATED
1, 30, EFFECTIVITY UPDATED (THROUGHOUT THE TEXT) 001-049, 051-099, 101-149, 34, 36-151-199, 201-299, 301-399, 37 401-499,
73-11-10 MOD.20011P0003 INCORPORATED ALL 401- 403, ELECTRICS- GENERATION- DISTRIBUTION-405, 407-V.U.'S AND AVIONICS- DEFINE SYSTEMS OF 416 THE BASIC AIRCRAFT-
CORRECTION/ADDITION/AMPLIFICATION ALL REVISED PROCEDURE LAYOUT IMPROVED/MATERIAL RELOCATED ALL MODIFIED MALFUNCTION WORDING STRUCTURE ALL
73-11-10 EFFECTIVITY UPDATED 624- 626 EFFECTIVITY UPDATED (THROUGHOUT THE TEXT) 106-149, 212-299, 301-399, 401-499,
73-11-10 MOD.20011P0003 INCORPORATED ALL
801- 806 ELECTRICS- GENERATION- DISTRIBUTION-V.U.'S AND AVIONICS- DEFINE SYSTEMS OF
THE BASIC AIRCRAFT-LAYOUT IMPROVED/MATERIAL RELOCATED ALL
73-11-49 CORRECTION/ADDITION/AMPLIFICATION ALL 401- 402, ADDED CLOSING OF THE LP FUEL VALVE 407, 409-LAYOUT IMPROVED/MATERIAL RELOCATED ALL 410
73-HIGHLIGHTS Page 1 of REVISION NO. 30 Aug 01/05
CES
F 『
E C F M E
E E
E 56-5B E
E E
CH/SE/SU C REASON FOR CHANGE EFFECTIVITY PAGES
73-11-50 MOD.20011P0003 INCORPORATED
401- 403, ELECTRICS- GENERATION- DISTRIBUTION-
408- 409, V.U.'S AND AVIONICS- DEFINE SYSTEMS OF
413 THE BASIC AIRCRAFT-
CORRECTION/ADDITION/AMPLIFICATION
DELETED "FIRE SHUT OFF VALVE" TEST.
LAYOUT IMPROVED/MATERIAL RELOCATED
73-20-00 EFFECTIVITY UPDATED
1,A021, EFFECTIVITY UPDATED (THROUGHOUT THE TEXT)
A024,A026-
A029
73-21-10 MOD.20011P0003 INCORPORATED
401- 403, ELECTRICS- GENERATION- DISTRIBUTION-
416, 424- V.U.'S AND AVIONICS- DEFINE SYSTEMS OF
426 THE BASIC AIRCRAFT-
CORRECTION/ADDITION/AMPLIFICATION
ADDED CAUTIONS
LAYOUT IMPROVED/MATERIAL RELOCATED
73-21-60 EFFECTIVITY UPDATED
402- 403, EFFECTIVITY UPDATED (THROUGHOUT THE TEXT)
410, 414-
415, 418
73-21-60 EFFECTIVITY UPDATED
511- 512, EFFECTIVITY UPDATED (THROUGHOUT THE TEXT)
514, 516-
517, 519,
522- 523,
525, 527-
528, 530,
532- 533,
535, 537-
540
73-21-90 EFFECTIVITY UPDATED
401, 405- EFFECTIVITY UPDATED (THROUGHOUT THE TEXT)
407, 409-
411
73-21-90 EFFECTIVITY UPDATED
501- 505, EFFECTIVITY UPDATED (THROUGHOUT THE TEXT)
510- 512,
514- 525
73-25-00 EFFECTIVITY UPDATED
CES
ALL
ALL
ALL
063-099, 106-149, 153-199, 205-299, 301-399, 401-499,
ALL
ALL
ALL
051-055, 057-057, 059-060,106-149, 159-199, 210-299,301-399, 401-499,
051-055, 057-057, 059-060,106-149, 212-299, 301-399,401-499,
063-099, 106-149, 153-199,205-299, 301-399, 401-499,
063-099, 106-149, 153-199,205-299, 301-399, 401-499,
73-HIGHLIGHTS Page 2 of REVISION NO. 30 Aug 01/05CH/SE/SU C REASON FOR CHANGE EFFECTIVITY PAGES
F 『
E C F M E
E E
E 56-5B E
E E
76, 79, EFFECTIVITY UPDATED (THROUGHOUT THE TEXT)
81
73-25-34 CIRCUIT BREAKER(S) DATA UPDATED
401- 402,
406
EFFECTIVITY UPDATED (THROUGHOUT THE TEXT)
73-25-34 MOD.30626K6443 INCORPORATED
501 AIR CONDITIONING-AIR COOLING-
INSTALL A NEW ECS
MOD.35481P9181 INCORPORATED
AIR CONDITIONNING-AIR COOLING-REMOVE
A318 TYPE ECS FROM A320 FURTHER TO MSCN
REJECTION. ANTI-MOD TO MOD 33780
MOD.35482P9182 INCORPORATED
AIR CONDITIONNING-AIR COOLING-REMOVE
A318 TYEP ECS FROM A321 FURTHER TO MSCN
REJECTION. ANTI-MOD OF MOD 33827
CIRCUIT BREAKER(S) DATA UPDATED
中国航空网 www.aero.cn
航空翻译 www.aviation.cn
本文链接地址:A320飞机维护手册 AMM 发动机燃油和控制 ENGINE FUEL AND CONTRO