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时间:2011-03-29 09:34来源:蓝天飞行翻译 作者:航空
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 2 If the fault continues during the subsequent flights:
_
 - replace the ECU (4000KS) (Ref. AMM TASK 73-21-60-000-001) and (Ref. AMM TASK 73-21-60-400-001).
 3 If the fault continues during the subsequent flights:
_
 - replace the HJ7 harness (Ref. AMM TASK 73-21-50-000-040) and (Ref. AMM TASK 73-21-50-400-040).
R (b) If the HMU part number is 8061-526 (GE SPEC 1348M79P08) or R higher:
 - disconnect the HJ7 harness from the HMU receptacle (HMU-A) (located in the left core compartment)

 - visually examine the HMU receptacle and the HJ7 harness connector for damaged pins or contamination (Ref. AMM TASK 73-21-50-210-001).


 1 If harness connector or HMU receptacle is damaged:
_ - repair or replace as required.
 2 If no damage is found:
_
 - do an electrical resistance test through the HMU receptacle between: . pins 21 and 41 (< 5 ohms) . pins 21 and 8 (> 10 megohms) . pin 21 and the ground (> 10 megohms).
 a If the resistance values are out of the specified limits:
_
 - replace the HMU (Ref. AMM TASK 73-21-10-000-002) and (Ref. AMM TASK 73-21-10-400-002).
 b If the resistance values are in the specified limits:
_ - reconnect the HJ7 harness
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 - disconnect the HJ7 harness from the ECU (4000KS) receptacle

 - visually examine the ECU (4000KS) receptacle and the HJ7 harness connector for damaged pins or contamination (Ref. AMM TASK 73-21-50-210-001).


 c If harness connector or ECU receptacle is damaged:
_ - repair or replace as required.
 d If no damage is found:
_
 - do an electrical resistance test through the HMU receptacle between: . pins 21 and 41 (< 5 ohms) . pins 21 and 8 (> 10 megohms) . pin 21 and the ground (> 10 megohms).
 e If the resistance values are in the specified limits:
_
 - replace the ECU (4000KS) (Ref. AMM TASK 73-21-60-000-001) and (Ref. AMM TASK 73-21-60-400-001).
 f If the resistance values are out of the specified limits:
_
 - replace the HJ7 harness (Ref. AMM TASK 73-21-50-000-040) and (Ref. AMM TASK 73-21-50-400-040).
 3 If the fault continues during the subsequent flights:
_
 - remove the HMU (Ref. AMM TASK 73-21-10-000-002)

 - inspect main fuel pump shaft.


 a If damaged/broken or worn:
_
 - replace the main fuel pump (Ref. AMM TASK 73-11-10-000-003) and (Ref. AMM TASK 73-11-10-400-003).
 b If not damaged/broken or worn:
_
 - replace the HMU (Ref. AMM TASK 73-21-10-000-002) and (Ref. AMM TASK 73-21-10-400-002).
 B. Do the test given in Para. 3.A.
 (1) No additional maintenance action is required if the fault is not confirmed.

 (2) Repeat the fault isolation procedure if the fault continues.


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 TASK 73-20-00-810-838
 Loss of the HMU Overspeed Governor - Engine 2 - Channel A
 1. Possible Causes
_______________
R - Hydromechanical Unit (HMU)
 - Main Fuel Pump (MFP)

 - ECU (4000KS)

 - HJ7 harness


 2. Job Set-up Information
______________________
 A. Referenced Information
 -------------------------------------------------------------------------------REFERENCE DESIGNATION -------------------------------------------------------------------------------
AMM 71-00-00-710-003 Engine Automatic Start AMM 73-11-10-000-003 Removal of the Fuel Pump and Filter Assembly AMM 73-11-10-400-003 Installation of the Fuel Pump and Filter Assembly AMM 73-21-10-000-002 Removal of the Hydromechanical Unit (HMU) AMM 73-21-10-400-002 Installation of the Hydromechanical Unit (HMU) AMM 73-21-50-000-040 Removal of the HJ7 Harness AMM 73-21-50-210-001 Visual Inspection of the Wiring Harness AMM 73-21-50-400-040 Installation of the HJ7 Harness AMM 73-21-60-000-001 Removal of the Electronic Control Unit (ECU) AMM 73-21-60-400-001 Installation of the Electronic Control Unit (ECU)
 3. Fault Confirmation
__________________
 A. Perfom an engine start (Ref. AMM TASK 71-00-00-710-003).
 4. Fault Isolation
_______________
R A. This fault is generated if an Overspeed Governor (OSG) switch position R fault is detected during an engine start. This fault can be caused by a R failed switch in the HMU, an open or short circuit in the HJ7 harness, R low fuel pressure to the HMU, or a failed main fuel pump shaft.
 
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