- replace the ELAC-1 (2CE1) (Ref. AMM TASK 27-93-34-000-001) and (Ref. AMM TASK 27-93-34-400-001).
(1) If the fault continues:
- do the trouble shooting procedure (Ref. TASK 31-32-00-810-932) related to the DSI 31 discret input signal of the ELAC 1 MON, SEC 1 MON and ELAC 2 (Ref. ASM 27-93/12) and (Ref. ASM 27-93/13).
「一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一1 EFF : ALL ∞∞27-40-00∞∞∞∞∞∞∞∞∞∞Page 208
May 01/00 CESR (2) If the fault continues:
- do a check of the wiring from the DSI-31 signal of the ELAC 1 (2CE1) to the first terminal block, COM part and MON part (Ref. ASM 27-93/12).
(a) If there is no continuity, repair the wiring.
(b) If there is continuity:
- do a check of the wiring from the overriding signal of the THS actuator (9CE) to the first terminal block (Ref. ASM 27-93/12).
1 If there is no continuity, repair the wiring.
_
2 If there is continuity:
_
- replace the pitch trim actuator (Ref. AMM TASK 27-44-57-000-001) and (Ref. AMM TASK 27-44-57-400-001).
B. Do the tests given in Para. 3.
Incorrect Position of the THS for the SEC 2
1. Possible Causes
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- RELAY-PITCH TRIM ACTUATOR MOTOR 3 SPLY (36CE3)
- SEC-2 (1CE2)
- electronic module N.3 of the pitch trim actuator
- monitor position transducer of the THS actuator
- RLY-PITCH TRIM ACTR MOT 3 SPLY (36CE3)
- wiring from the relay (36CE3), pin A/X2 to the ground
- wiring from the relay (36CE3) to the SEC 2 (1CE2)
- wiring from the THS actuator pin D/J to the ground
- wiring from the relay (36CE3) to the THS actuator (9CE)
- wiring from the relay (36CE3) A/A2 to the C/B (19CE3)
- wiring of the XDCR MON MOT 3 (V1, V2) signal
2. Job Set-up Information
______________________
A. Referenced Information
-------------------------------------------------------------------------------REFERENCE DESIGNATION -------------------------------------------------------------------------------
R IPC 27920803 AMM 27-44-56-000-001 Removal of the Position Transducer from the THS Actuator 9CE AMM 27-44-56-400-001 Installation of the Position Transducer to the THS Actuator 9CE AMM 27-44-57-000-001 Removal of the Pitch Trim Actuator from the THS Actuator 9CE AMM 27-44-57-400-001 Installation of the Pitch Trim Actuator to the THS
Actuator 9CE
AMM 27-94-34-000-001 Removal of the SEC (1CE1,1CE2,1CE3)
AMM 27-94-34-400-001 Installation of the SEC (1CE1,1CE2,1CE3)
AMM 27-96-00-710-022 Operational Test of the THS Actuator Electrical
Control (Activation for BITE Test) AMM 27-96-00-740-001 BITE Test of the EFCS (Ground Scanning) R ASM 27-94/13
3. Fault Confirmation
__________________
A. Test
(1) Do the operational test of the THS actuator electrical control (Ref. AMM TASK 27-96-00-710-022).
NOTE : Do the ground setting only with the SEC 2.
____
「一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一一1 EFF : ALL ∞∞27-40-00∞∞∞∞∞∞∞∞∞∞Page 210
Aug 01/00 CES
(2) Do the BITE test of the EFCS (ground scanning) (Ref. AMM TASK 27-96-00-740-001).
4. Fault Isolation
_______________
A. If the BITE test gives the maintenance message:
THS ACTR POS ERROR 9CE OF SEC2
R (1) Remove the RELAY-PITCH TRIM ACTUATOR MOTOR 3 SPLY (36CE3) (Ref. IPC R 27920803).
(2) Do a check of the resistance between pins X1 and X2.
(a) If the resistance is less than 280 ohms:
- replace the RELAY-PITCH TRIM ACTUATOR MOTOR 3 SPLY (36CE3)
- replace the SEC-2 (1CE2) (Ref. AMM TASK 27-94-34-000-001) (Ref. AMM TASK 27-94-34-400-001).
(b) If the resistance is more than 400 ohms:
- replace the RELAY-PITCH TRIM ACTUATOR MOTOR 3 SPLY (36CE3).
(c) If the resistance is between 280 and 400 ohms:
- install the RELAY-PITCH TRIM ACTUATOR MOTOR 3 SPLY (36CE3)
- see para (3).
(3) If the fault continues:
- replace the SEC-2 (1CE2) (Ref. AMM TASK 27-94-34-000-001) and (Ref. AMM TASK 27-94-34-400-001).
(4) If the fault continues:
- replace the electronic module N.3 of the pitch trim actuator (Ref. AMM TASK 27-44-57-000-001) and (Ref. AMM TASK 27-44-57-400-001). 中国航空网 www.aero.cn 航空翻译 www.aviation.cn 本文链接地址:A320 Trouble Shooting Manual 排故手册 飞行操纵 1(75)