Loss of the Left Elevator because of its Two Servocontrols
1. Possible Causes
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- SERVO CTL-L ELEVATOR, INBD G (34CE1)
- SERVO CTL-L ELEVATOR, OUTBD B (34CE3)
2. Job Set-up Information
______________________
A. Referenced Information
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REFERENCE DESIGNATION
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AMM 27-34-00-200-001 Check of the Elevator Servo Controls and Hinge
Bearings for too much Play and Condition
AMM 27-34-00-710-001 Operational Test of the Elevator and Hydraulic
Actuation
R AMM 27-34-51-000-001 Removal of the Elevator Servo Control
R AMM 27-34-51-400-001 Installation of the Elevator Servo Control AMM 27-96-00-710-008 Operational Test of the Damping Measurement (Elevator)
3. Fault Confirmation
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A. Test
(1) Not applicable, you cannot confirm this fault on the ground.
4. Fault Isolation
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A. Do a check of the left elevator servocontrols and hinge bearings for too much play and condition (Ref. AMM TASK 27-34-00-200-001).
(1) Do an operational test of the damping measurement (Elevator) (Ref. AMM TASK 27-96-00-710-008):
- if the result of the test is not in the tolerances, see Para. (a)
- if the result of the test is in the tolerances, see Para. (b).
(a) Replace the SERVO CTL-L ELEVATOR, INBD G (34CE1) and the SERVO CTL-L ELEVATOR, OUTBD B (34CE3) of the left elevator (Ref. AMM TASK 27-34-51-000-001) and (Ref. AMM TASK 27-34-51-400-001).
NOTE : The resistance of primary and secondary windings must be
____ between 30 ohms and 500 ohms.
(b) Do the operational test of the elevator and hydraulic actuation (Ref. AMM TASK 27-34-00-710-001).
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Aug 01/03 CES Loss of the Signal of the Left Elevator Position Transducer (MON) by the SEC 1
1. Possible Causes
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- SEC-1 (1CE1)
- wiring of the POS XDCR MON (ANI 2-1) signal from the SEC 1 (1CE1) MON part to the first terminal block
2. Job Set-up Information
______________________
A. Referenced Information
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REFERENCE DESIGNATION
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27-90-00-810-818 Loss of the ACS1 Signal of the SEC1 MON Side
AMM 27-94-34-000-001 Removal of the SEC (1CE1,1CE2,1CE3)
AMM 27-94-34-400-001 Installation of the SEC (1CE1,1CE2,1CE3)
AMM 27-96-00-710-020 Operational Test of the Side Stick Assembly
(Activation for the BITE Test) R AMM 27-96-00-740-001 BITE Test of the EFCS (Ground Scanning) ASM 27-94/07
3. Fault Confirmation
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A. Test
(1) Do the operational test of the side stick assembly (Activation for the BITE test) (Ref. AMM TASK 27-96-00-710-020).
NOTE : Before you start the operational test procedure, release the
____ FLT CTL/ELAC 1, FLT CTL/ELAC 2 and FLT CTL/SEC 2 pushbutton switches (on these pushbutton switches the OFF legends come on).
(2) Do the BITE test of the EFCS (ground scanning) (Ref. AMM TASK 27-96-00-740-001).
(a) If the ground scanning gives the maintenance message: SEC1 OR WIRING FROM L ELEV POS MON XDCR
- refer to Para. Fault Isolation.
(b) If the ground scanning gives at least two maintenance messages of the list below: SEC1 OR WIRING FROM L ELEV POS MON XDCR SEC1 OR WIRING FROM R ELEV POS MON XDCR SEC1 MON OR WIRING FROM THS ACTR XDCR2 9CE SEC1 OR WIRING FROM L G ELEV MODE XDCR 34CE1 SEC1 OR WIRING FROM R Y ELEV MODE XDCR 34CE2 中国航空网 www.aero.cn 航空翻译 www.aviation.cn 本文链接地址:A320 Trouble Shooting Manual 排故手册 飞行操纵 1(39)